QFR No - 8000779380
Defect Details
NC No. 8000779380
NC Date 10/03/2022
NC Submission Date
Part No. F1FA01333M
Part Name FORK PIPE MACHINED-K86A
Supplier Name & Code 101187-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1146-ETL Suspension Narasapura
Defect Details DIMN.U/SIZE.-TOTAL LENGTH LESS ISSUE
 
1. Problem Description
Defect Description front fork K86 fork pipe Specification = Total Length Specification = – 288.3±0.2mm,Observation= Total Length – 285.39 mm, total length less issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo 5btumtx43lb0oa45ujucrky4.xlsx
Supplier Communication Details
Quality Head Email ID AmitVD@tii.murugappa.com
Plant Head/CEO Email ID guptaajay@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1320
0
0
800
0
2120
Check Qty
1320
0
0
800
0
2120
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Available lot at Endurance checked 100% - No rejection
 
3. Process Flow
Process Flow Description
Cut to length CNC Machining 1 CNC Machining 2 Drilling Final Inspection Packing & Despatch
 
4. Process Details
Process / Operation CNC Machining
Outsource Yes
Machine / Cell CNC Machine
Machine / Cell No. M08
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineLoose burr got struck at the endVerified with Loose burr at the edge condition & Observed Length undersize based on the burr thkO
MaterialRM Tube length undersizeRM tube verified & found OKX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 Total height under size up to 3mm
Why 2 Part moved at front side
Why 3 Improper face butting
Why 4 Machining burr sticked at butting face
Why 5 Air cleaning process not done properly
Root Cause (Occurance) Air cleaning process not done properly
 
Root Cause Analysis (Outflow)
Why 1 Skipped from final inspection
Why 2 Sample inspection only
Why 3 As defined in the Existing System
Why 4
Why 5
Root Cause (Outflow) Sample inspection only
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAir line provided in the Clamping chuckOhm Industry04/07/202224/03/2022Completed
Outflow100% inspection implemented at process and FIOhm Industry11/03/202211/03/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Final Inspection 100% Inspection added
Inspection Method Other
Other Inspection Method Dial Gauge
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Manual Air cleaning
10_Occurance_Before.xlsx
Occurance (After) Air cleaning Nozzle introduced
10_Occurance_After.xlsx
Outflow (Before) Sample inspection
10_Outflow_Before.xlsx
Outflow (After) 100% Inspection at Final Inspection
10_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant K86 Model
 
12. Document Review
Documents PFMEA, WISOP
Specify Other Document Q- Alert displayed
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission