QFR No - 8000779743
Defect Details
NC No. 8000779743
NC Date 12/03/2022
NC Submission Date
Part No. S1CW00512B
Part Name D NUT K0LA
Supplier Name & Code 100165-SAPTAGIRI INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details THREADING MISSING-DNUT WITHOUT THREADING
 
1. Problem Description
Defect Description K0LA rear D nut without threading issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 3
Is Defect Repeatative? No
Defect Sketch / Photo r4uioy4swlnu5yytx1sfjsju.xlsx
Supplier Communication Details
Quality Head Email ID quality@saptagirigroup.in
Plant Head/CEO Email ID quality@saptagirigroup.in
MD Email ID argandhi@saptagirigroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
12000
0
13500
5200
40700
Check Qty
10000
12000
0
13500
5200
40700
NG Qty
0
0
0
25
0
25
 
Scrap 13
Rework 0
Under Deviation 0
Containment Action
We have checked In house and M/S ETL end
 
3. Process Flow
Process Flow Description
Raw Material Inward Sheet Shearing Blanking & Center Piercing Both side chamfer Tapping Plating Final Inspection Packing/storing
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Machine No 1
Machine / Cell No. Machine No 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolPunch NGPunch Worn out.O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50
7. Root Cause Analysis (Occurance)
Why 1 D`nut found Go not pass
Why 2 Punch Worn out.
Why 3 Before threading Id undersize observed 8.65mm Instead of 8.75mm.
Why 4 Tool History card not updated
Why 5
Root Cause (Occurance) Before threading Id undersize observed 8.65mm Instead of 8.75mm.
 
Root Cause Analysis (Outflow)
Why 1 Punch Replace with New one with size 8.75mm.
Why 2 Tool history card maintain.
Why 3 Sampling qty. increases for thread inspection for inprocess & final inspection 100 nos/lot instead of 50 nos/lot
Why 4
Why 5
Root Cause (Outflow) Sampling qty. increases for thread inspection for inprocess & final inspection 100 nos/lot instead of 50 nos/lot
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
-------
Type Countermeasure Details Responsibility Target Date Actual Date Status
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details final inspection 100 nos/lot instead of 50 nos/lot
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50
10. Evidance of Countermeasure
Occurance (Before) Punch wear out NOGO Pass
14_Occurance_Before.pptx
Occurance (After) Punch Replace Dimn.
14_Occurance_After.pptx
Outflow (Before) Less sampling frequency
14_Outflow_Before.pdf
Outflow (After) sampling frequency Increase
14_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Saptagiri Engg. Machine No 1
 
12. Document Review
Documents WISOP
Specify Other Document N/A
 
13. Effectiveness Of Action
Reviewed Quantity 15000
Reason for submission reviewed 15000 numbers no thread miss found ok