QFR No - 8000779743
Defect Details
NC No. | 8000779743 |
NC Date | 12/03/2022 |
NC Submission Date | |
Part No. | S1CW00512B |
Part Name | D NUT K0LA |
Supplier Name & Code | 100165-SAPTAGIRI INDUSTRIES |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | THREADING MISSING-DNUT WITHOUT THREADING |
1. Problem Description
Defect Description | K0LA rear D nut without threading issue |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 3 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | r4uioy4swlnu5yytx1sfjsju.xlsx |
Supplier Communication Details
Quality Head Email ID | quality@saptagirigroup.in |
Plant Head/CEO Email ID | quality@saptagirigroup.in |
MD Email ID | argandhi@saptagirigroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
10000
|
12000
|
0
|
13500
|
5200
|
40700
|
Check Qty |
10000
|
12000
|
0
|
13500
|
5200
|
40700
|
NG Qty |
0
|
0
|
0
|
25
|
0
|
25
|
Scrap | 13 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
We have checked In house and M/S ETL end |
3. Process Flow
Process Flow Description |
---|
Raw Material Inward Sheet Shearing Blanking & Center Piercing Both side chamfer Tapping Plating Final Inspection Packing/storing |
4. Process Details
Process / Operation | Tapping |
Outsource | No |
Machine / Cell | Machine No 1 |
Machine / Cell No. | Machine No 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Punch NG | Punch Worn out. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 |
7. Root Cause Analysis (Occurance)
Why 1 | D`nut found Go not pass |
Why 2 | Punch Worn out. |
Why 3 | Before threading Id undersize observed 8.65mm Instead of 8.75mm. |
Why 4 | Tool History card not updated |
Why 5 | |
Root Cause (Occurance) | Before threading Id undersize observed 8.65mm Instead of 8.75mm. |
Root Cause Analysis (Outflow)
Why 1 | Punch Replace with New one with size 8.75mm. |
Why 2 | Tool history card maintain. |
Why 3 | Sampling qty. increases for thread inspection for inprocess & final inspection 100 nos/lot instead of 50 nos/lot |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Sampling qty. increases for thread inspection for inprocess & final inspection 100 nos/lot instead of 50 nos/lot |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | final inspection 100 nos/lot instead of 50 nos/lot |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 |
10. Evidance of Countermeasure
Occurance (Before) |
Punch wear out NOGO Pass 14_Occurance_Before.pptx |
Occurance (After) |
Punch Replace Dimn. 14_Occurance_After.pptx |
Outflow (Before) |
Less sampling frequency 14_Outflow_Before.pdf |
Outflow (After) |
sampling frequency Increase 14_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Saptagiri Engg. Machine No 1 |
12. Document Review
Documents | WISOP |
Specify Other Document | N/A |
13. Effectiveness Of Action
Reviewed Quantity | 15000 |
Reason for submission | reviewed 15000 numbers no thread miss found ok |