QFR No - 8000780349
Defect Details
NC No. 8000780349
NC Date 18/03/2022
NC Submission Date
Part No. F1GN01102B
Part Name MAIN SPRING K86A
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1146-ETL Suspension Narasapura
Defect Details LENGTH UNDERSIZE-TOTAL LENGTH LESS ISSUE
 
1. Problem Description
Defect Description main spring total length less
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo ilia2cr5nev23hks14ow220m.xlsx
Supplier Communication Details
Quality Head Email ID arun@helicalsprings.in
Plant Head/CEO Email ID shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
8000
0
0
12000
30000
Check Qty
10000
8000
0
0
12000
30000
NG Qty
5
0
0
0
0
5
 
Scrap 5
Rework 0
Under Deviation 0
Containment Action
100 % inspection done at ETL, warehouse & FG.
 
3. Process Flow
Process Flow Description
RAW MATERIAL, COILING, STRESS RELEIVING-1, END GRINDING, SHOT PEENING, SCRAGGING, LENGTH,OD & WAVYNESS CHECKING, STRESS RELEIVING-2, Surface Finish- Oiling , PDI, Packing & Dispatch.
 
4. Process Details
Process / Operation Coiling
Outsource No
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper length settingImproper locking of length gaugeX
MaterialAs per DrawingRMTC checked found okO
MachineHerdonFound okO
ManUnskilled operatorSkill Matrix checked found okO
MethodImproper material handingSetup part mix with ok partX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 length short
Why 2 During setup length short spring coiled
Why 3 Setup quantity mix with the ok material
Why 4 No provision was available for setup part storage
Why 5
Root Cause (Occurance) No provision was available for setup part storage
 
Root Cause Analysis (Outflow)
Why 1 length short
Why 2 Length gauge setting disturbed
Why 3 Improper locking of Length gauge
Why 4 No cross check method for length gauge verification
Why 5
Root Cause (Outflow) No cross check method for length gauge verification
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Yellow bin introduced at coiling to keep suspected/setup part 2. OPL displayed at coiling 3. Training provided to the operator and recorded the sameMr.Mahadev23/03/202222/03/2022Completed
Outflow1. Free length tolerance band reduced from +4.0 mm to +3.50 mm 2. Dedicated length gauge will be introduced for K0LA main spring (fixed type) 3. Control plan changed and updatedQuality24/03/202223/03/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No Change
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 25/Lot
10. Evidance of Countermeasure
Occurance (Before) Yellow Bin not available.
21_Occurance_Before.pdf
Occurance (After) .1. Yellow bin introduced at coiling to keep suspected/setup part 2. .OPL displayed at coiling 3.Training provided to to the operator and recorded the same
21_Occurance_After.pdf
Outflow (Before) Free length Gauge band 4.0 mm
21_Outflow_Before.pdf
Outflow (After) 1. The free length tolerance band was reduced from +4.0 mm to +3.50 mm 2. A dedicated length gauge will be introduced for K0LA main spring (fixed type)
21_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Similar Modal
 
12. Document Review
Documents WISOP
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 15000
Reason for submission reviewed 15000 numbers no length issue found ok