QFR No - 8000782049
Defect Details
NC No. 8000782049
NC Date 27/03/2022
NC Submission Date
Part No. F1GN01102B
Part Name MAIN SPRING K86A
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1136-ETL Suspension Sanand
Defect Details HIGHT U/SIZE.-TOTAL HIGHT UNDERSIZE
 
1. Problem Description
Defect Description Total Length Under Size and Over Size i.e. 244.42, 213.11 mm
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 231
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID arun@helicalsprings.in
Plant Head/CEO Email ID shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
12000
16000
0
5800
6000
39800
Check Qty
10000
16000
0
5800
6000
37800
NG Qty
231
42
0
58
0
331
 
Scrap 273
Rework 58
Under Deviation 0
Containment Action
100% inspection done for length at ETL & Warehouse.
 
3. Process Flow
Process Flow Description
Raw Material Receipt & Inspection, Coiling, Stress Relieving, End Grinding, Shot Peening, Scragging, Length & Wavyness checking, Strain-aging, Surface Finish- Oiling, Final Inspection/ PDI, Packing, Dispatch
 
4. Process Details
Process / Operation Coiling
Outsource No
Machine / Cell NA
Machine / Cell No. CNC Coiling
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operatorSkill Matrix checked found okO
MethodImproper length settingImproper locking of length gaugeX
MaterialAs per DrawingRMTC checked found okO
Method1.Improper material handingSetup part mix with ok partX
MachineHerdonFound okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 29 / 10000
7. Root Cause Analysis (Occurance)
Why 1 length short
Why 2 During setup length short spring coiled
Why 3 Setup quantity mix with the ok material
Why 4 No provision was available for setup part storage
Why 5
Root Cause (Occurance) No provision was available for setup part storage
 
Root Cause Analysis (Outflow)
Why 1 length short
Why 2 Length gauge setting disturbed
Why 3 Improper locking of Length gauge
Why 4 No cross check method for length gauge verification
Why 5
Root Cause (Outflow) No cross check method for length gauge verification
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1.Free length tolerance band reduced from +4.0 mm to +3.50 mm 2.Dedicated length gauge will be introduced for K0LA main spring (fixed type) 3.Control plan changed and updatedArun Kumar30/03/202228/03/2022Completed
Occurance1.Yellow bin introduced at coiling to keep suspected/setup part 2.OPL displayed at coiling 3.Training provided to the operator and recorded the sameArun Kumar30/03/202224/03/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Free length tolerance band reduced from +4.0 mm to +3.50 mm
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 29 / 10000
10. Evidance of Countermeasure
Occurance (Before) Yellow bin not Available
25_Occurance_Before.pdf
Occurance (After) Yellow bin introduced at coiling to keep suspected/setup part
25_Occurance_After.pdf
Outflow (Before) Free length gauge tolerance 4.00 mm
25_Outflow_Before.pdf
Outflow (After) Free length tolerance band reduced from +4.0 mm to +3.50 mm
25_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Similar Part.
 
12. Document Review
Documents
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Verified and found effective till date