QFR No - 8000782060
Defect Details
NC No. 8000782060
NC Date 27/03/2022
NC Submission Date
Part No. S2HT52107B
Part Name OUTER SPRING K0PG
Supplier Name & Code 101048-STUMPP SCHUELE AND SOMAPPA SPR
ETL Plant 1136-ETL Suspension Sanand
Defect Details DIMETER UNDERSIZE-INNERDIA UNDERSIZE
 
1. Problem Description
Defect Description ID Under Size
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID pathan.ak@ssssprings.com
Plant Head/CEO Email ID udham.singh@ssssprings.com
MD Email ID rln@ssssprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2016
0
0
0
1200
3216
Check Qty
2016
0
0
0
1200
3216
NG Qty
1
0
0
0
1
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
Available internal parts segregated 100 %. Available Qty of 1200 nos checked, 1 part found having ID undersize. All the springs will be provided with small line on small ID end for next 3 lots.
 
3. Process Flow
Process Flow Description
Recipt & inspection - Visual - Storage of material - Winding RH - Stress Relieving - Grinding - Shot peening - Scragging - Lo,OD,e1 & bend sorting and correction - Stress Relieving (LTA) - Powder coating - Final Inspection - Packing
 
4. Process Details
Process / Operation Grinding
Outsource No
Machine / Cell SGM-2 (Grinding machine)
Machine / Cell No. Grinding
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineWrong Set up during coilingVerified and found the correct setting was done.O
ManUnskilled OperatorSkilled operator deputed at coiling stageO
ToolWrong or damaged magazine plate at Grinding stageVerified and found the correct magazine plate for grinding of this partO
MethodWrong orientation of spring in Grinding bush.End moved inside due to wrong placement of spring in grinding bushX
MethodPart mix upVerified & found that NG parts mixed-up with OK parts.X
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Problem occur during grinding operation.
Why 2 Spring in Guide bush placed with wrong orientation (Bigger side down in place of upward)
Why 3 spring orientation during grinding not specified & documented
Why 4
Why 5
Root Cause (Occurance) spring orientation during grinding not specified & documented
 
Root Cause Analysis (Outflow)
Why 1 Problem occur during 100% ID inspection at powder coating.
Why 2 Captured ID tight parts mixed-up with Ok parts.
Why 3 Both the parts were kept nearby on inspection table by operator.
Why 4 No separator for the OK and NG parts at inspection table.
Why 5
Root Cause (Outflow) No separator for the OK and NG parts at inspection table.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWork instruction revised to add the spring orientation (Bigger side up) in Grinding bush during grinding operation & training provided to the operators accordingly.Mr. Dixit07/04/202207/04/2022Completed
OccuranceID inspection and Control added at Grinding Stage, Control plan revised for the same.Mr. Maulesh06/04/202206/04/2022Completed
OutflowSeparator provided on inspection table with proper identification to avoid mix-upMr. Shashank06/04/202206/04/2022Completed
OutflowAwareness training given to the operators to keep NG parts in red bin.Mr. Shashank07/04/202206/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling inspection for ID started at Grinding stage, control plan revised for the same.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No ID inspection at Grinding stage, Spring orientation in Grinding was not specified in Work instruction
26_Occurance_Before.pdf
Occurance (After) ID inspection started at Grinding stage, Control plan revised for the same. Work instruction revised to add the spring orientation (Bigger side up) in Grinding bush during grinding operation & training provided to the operators accordingly.
26_Occurance_After.jpg
Outflow (Before) OK and reworkable parts were kept at the same inspection table without any separator.
26_Outflow_Before.png
Outflow (After) Separator provided on inspection table to place OK and reworkable parts separate to avoid mix-up of OK and NG parts
26_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Inspection for ID started for all the OC springs.
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission Accepted