QFR No - 8000782061
Defect Details
NC No. 8000782061
NC Date 27/03/2022
NC Submission Date
Part No. 520CJ00102
Part Name COPPER WASHER
Supplier Name & Code 100152-GOLDY PRECISION STAMPINGS PVT.
ETL Plant 1136-ETL Suspension Sanand
Defect Details EXCESS CUT/SANDERING-CUT FROM EDGE
 
1. Problem Description
Defect Description Part Cut From OD
Detection Stage Inprocess
Problem Severity Function
NG Quantity 5
Is Defect Repeatative? Yes
Defect Sketch / Photo rfo2mvbruc002pra10ggh2kq.png
Supplier Communication Details
Quality Head Email ID quality@goldy.in
Plant Head/CEO Email ID mangesh.chaudhary@goldy.in
MD Email ID sidhesh.raikar@goldy.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
0
0
10000
0
20000
Check Qty
10000
0
0
10000
0
20000
NG Qty
5
0
0
0
0
5
 
Scrap 5
Rework 0
Under Deviation 0
Containment Action
Finish good qty 10000 Nos verify at visual inspection found ok.
 
3. Process Flow
Process Flow Description
10- RAW MATERIAL INSPECTION, 20-BLANKING, 30-ANNELING, 40-100% VISUAL INSPECTION, PACKING & FG STOCK, 50-FINAL INSPECTION & DISPATCH
 
4. Process Details
Process / Operation BLANKING
Outsource No
Machine / Cell PRESS MACHINE
Machine / Cell No. P-4
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator skillVerify opeartor skill as per Enducation & training, operator found trainedO
MethodBlanking method not okChecked method as per work instruction found okO
ToolTool not okVerify Tool condition, dowel pin found not okX
MachineMachine not okChecked Parameter checked founf okO
MaterialMaterial not okMaterial thickness width, hardness checked found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Outer Diameter cut found parts no- 520CJ00102
Why 2 Outer diameter cut during blanking while strip feeding
Why 3 Strip Overlap feed because toll dowel not control to overlap operation
Why 4 Dowel pin not ok, dowel pin height in sufficient
Why 5 NOT APPLICABLE
Root Cause (Occurance) Dowel pin not ok, dowel pin height in sufficient
 
Root Cause Analysis (Outflow)
Why 1 Outer diameter cut parts skipped in visual inspection
Why 2 Operator could not detect to cut parts
Why 3 Operator take more parts on table for visual inspection
Why 4 NOT APPLICABLE
Why 5 NOT APPLICABLE
Root Cause (Outflow) Operator take more parts on table for visual inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1) Dowel pin height increase more than 2 mm of thickness. (Height increase 3.5 against 1.5mm) 2) Operator verify pin height condition before start blanking.Vikas Divate / Rahul kandale28/03/202228/03/2022Completed
Outflow10-12 no`s parts checking started on visual inspection on tableRahul Pawar29/03/202229/03/2022Completed
OutflowTraining given to visual inspector for part inspectionRahul Pawar / Vikas Divate29/03/202229/03/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 10-12 no`s parts checking started on visual inspection on table
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Dowel pin not ok, dowel pin height in sufficient
27_Occurance_Before.pdf
Occurance (After) 1) Dowel pin height increase more than 2 mm of thickness. (Height increase 3.5 against 1.5mm) 2)Operator verify pin condition before start blanking.
27_Occurance_After.pdf
Outflow (Before) Operator take more parts on table for visual inspection
27_Outflow_Before.pdf
Outflow (After) 10-12 no`s parts checking started on visual inspection on table
27_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Cooper parts - 520CJ00502 & 520CJ00702
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document Before after
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Accepted