QFR No - 8000782143
Defect Details
NC No. | 8000782143 |
NC Date | 28/03/2022 |
NC Submission Date | |
Part No. | 580DV00102 |
Part Name | GEAR CONTROL PULLY H BAR ASSLY(24191184) |
Supplier Name & Code | 101086-PUNE POLYMERS PVT. LTD. |
ETL Plant | 1102-ETL L-6 Die Casting |
Defect Details | FITTMENT NOT OK.-HOLE SHIFT |
1. Problem Description
Defect Description | Diameter 2.2 Shift |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 669 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qa.waluj@punepolymers.com |
Plant Head/CEO Email ID | planthead.waluj@punepolymers.com |
MD Email ID | s.gupta@punepolymers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5000
|
0
|
0
|
1500
|
1500
|
8000
|
Check Qty |
5000
|
0
|
0
|
1500
|
1500
|
8000
|
NG Qty |
550
|
0
|
0
|
0
|
0
|
550
|
Scrap | 550 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % inspection done for all material in stock. |
3. Process Flow
Process Flow Description |
---|
In. molding - Inspection - packing - Dispatch |
4. Process Details
Process / Operation | Inj. molding |
Outsource | No |
Machine / Cell | Cell A |
Machine / Cell No. | Cell A |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Pin bent in mold. | Pin bent in mold. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 |
7. Root Cause Analysis (Occurance)
Why 1 | Fitment not ok |
Why 2 | Hole shift |
Why 3 | Pin bent in mold. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Pin bent in mold. |
Root Cause Analysis (Outflow)
Why 1 | Skipped from inspection. |
Why 2 | Not detected in sampling. |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Not detected in sampling. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Pin replaced in the mold. | PPPL | 15/04/2022 | 15/04/2022 | Completed |
Outflow | 100 % inspection | PPPL | 05/04/2022 | 05/04/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100 % inspection. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
Pin bent 30_Occurance_Before.xls |
Occurance (After) |
Pin replaced. 30_Occurance_After.xls |
Outflow (Before) |
Sampling inspection. 30_Outflow_Before.xls |
Outflow (After) |
100 % inspection. 30_Outflow_After.xls |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 50000 |
Reason for submission | Monitor for next one month & no issue observed |