QFR No - 8000782421
Defect Details
NC No. | 8000782421 |
NC Date | 31/03/2022 |
NC Submission Date | |
Part No. | 520PC03307 |
Part Name | UNDER BKT SUB-ASSY. K3 |
Supplier Name & Code | 100348-SINGLA FORGING |
ETL Plant | 1126-ETL Pantnagar |
Defect Details | POWDER COATING NOT OK-POWDER COATING UNCOVER |
1. Problem Description
Defect Description | Powder coating uncover in Under bracket at BAL |
Detection Stage | Customer End |
Problem Severity | Aesthetic |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | pntquality@singlaforging.in |
Plant Head/CEO Email ID | deepakgupta@singlaforging.com |
MD Email ID | jain@singlaforging.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
150
|
0
|
0
|
180
|
0
|
330
|
Check Qty |
150
|
0
|
0
|
180
|
0
|
330
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 0 |
Rework | 1 |
Under Deviation | 0 |
Containment Action |
---|
1-100% segregation of material lying at various stages to be done with OK confirmation marking 2-Quality Alert to be displayed at work station |
3. Process Flow
Process Flow Description |
---|
Operation No Operation 10 Receipt of Material 20 Receipt Inspection 30 Storage 40 VMC Machining-I 50 VMC Machining-II 60 VMC Machining-III 70 Slitting 80 Received material & Inspection 90 Pipe Pressing, 100 Welding 110 Powder Coating 120 Final Inspection 130 Packing 140 Dispatch |
4. Process Details
Process / Operation | Powder Coating |
Outsource | Yes |
Machine / Cell | Powder Coating cell |
Machine / Cell No. | Unmasking |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Method of unmasking not adequate | Checked and obserbed method of unmasking was not adeqate.i.e operator was unmasking the side id mask | X |
Method | Method of applying powder through gun not adequate | Checked and verfied that trained operator are applying powder through gun in booth | O |
Method | Insp method not adequate | Checked & verifed that inspector was doing the visual inspection | O |
Man | Unskilled/Unaware Inspector/operator | Checked & verified that skilled inspector/operator are working but having some unawareness | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Method of unmasking of side ID of powder coated parts was not adequate. |
Why 2 | Operator was removing the masking from the side ID directly with hand before moving of powder coated parts in the oven.. |
Why 3 | No other provisions for removing the masking from the powder coated part not available. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | No other provisions for removing the masking from the powder coated part not available. |
Root Cause Analysis (Outflow)
Why 1 | Powered coated uncover part skipped from the final stage |
Why 2 | Part was not detected in the final inspection stage. |
Why 3 | Inspector was not aware. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector was not aware. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1-Method of removing the masking will be defined i.e. masking will be removed through plastic stick. | Mukesh Kumar Singh | 06/04/2022 | 04/04/2022 | Completed |
Occurance | 2-WI for removing of masking to be made & displayed. | Mukesh Kumar Singh | 06/04/2022 | 04/04/2022 | Completed |
Outflow | 1-Awareness training to be provided to the final inspector. | Sarvesh Kumar | 06/04/2022 | 05/04/2022 | Completed |
Outflow | 100% visual inspection is started at M/s steel Engineers end with proper identification marking. | Mukesh Kumar Singh | 06/04/2022 | 02/04/2022 | Completed |
Outflow | Powder coating defects matrix to be made & displayed at final inspection stage and training to be provided | Sunil | 04/04/2022 | 04/04/2022 | Completed |
Occurance | 3-OJT to be provided for removing the masking. | Mukesh Kumar Singh | 06/04/2022 | 05/04/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% visual inspection is started at M/s steel Engineers end with proper identification marking. |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Masking pull directly from the part before oven through hand 35_Occurance_Before.xlsx |
Occurance (After) |
Method of removing the masking will be defined i.e masking will be removed through plastic stick. 35_Occurance_After.pdf |
Outflow (Before) |
Not Available 35_Outflow_Before.pdf |
Outflow (After) |
Powder coating defects matrix to be made & displayed at final inspection stage and training to be provided. 35_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | ALL UBA |
12. Document Review
Documents | WISOP |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | OK |