QFR No - 8000782421
Defect Details
NC No. 8000782421
NC Date 31/03/2022
NC Submission Date
Part No. 520PC03307
Part Name UNDER BKT SUB-ASSY. K3
Supplier Name & Code 100348-SINGLA FORGING
ETL Plant 1126-ETL Pantnagar
Defect Details POWDER COATING NOT OK-POWDER COATING UNCOVER
 
1. Problem Description
Defect Description Powder coating uncover in Under bracket at BAL
Detection Stage Customer End
Problem Severity Aesthetic
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID pntquality@singlaforging.in
Plant Head/CEO Email ID deepakgupta@singlaforging.com
MD Email ID jain@singlaforging.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
150
0
0
180
0
330
Check Qty
150
0
0
180
0
330
NG Qty
1
0
0
0
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
1-100% segregation of material lying at various stages to be done with OK confirmation marking 2-Quality Alert to be displayed at work station
 
3. Process Flow
Process Flow Description
Operation No Operation 10 Receipt of Material 20 Receipt Inspection 30 Storage 40 VMC Machining-I 50 VMC Machining-II 60 VMC Machining-III 70 Slitting 80 Received material & Inspection 90 Pipe Pressing, 100 Welding 110 Powder Coating 120 Final Inspection 130 Packing 140 Dispatch
 
4. Process Details
Process / Operation Powder Coating
Outsource Yes
Machine / Cell Powder Coating cell
Machine / Cell No. Unmasking
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodMethod of unmasking not adequateChecked and obserbed method of unmasking was not adeqate.i.e operator was unmasking the side id maskX
MethodMethod of applying powder through gun not adequateChecked and verfied that trained operator are applying powder through gun in boothO
MethodInsp method not adequateChecked & verifed that inspector was doing the visual inspectionO
ManUnskilled/Unaware Inspector/operatorChecked & verified that skilled inspector/operator are working but having some unawarenessX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Method of unmasking of side ID of powder coated parts was not adequate.
Why 2 Operator was removing the masking from the side ID directly with hand before moving of powder coated parts in the oven..
Why 3 No other provisions for removing the masking from the powder coated part not available.
Why 4
Why 5
Root Cause (Occurance) No other provisions for removing the masking from the powder coated part not available.
 
Root Cause Analysis (Outflow)
Why 1 Powered coated uncover part skipped from the final stage
Why 2 Part was not detected in the final inspection stage.
Why 3 Inspector was not aware.
Why 4
Why 5
Root Cause (Outflow) Inspector was not aware.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1-Method of removing the masking will be defined i.e. masking will be removed through plastic stick.Mukesh Kumar Singh06/04/202204/04/2022Completed
Occurance2-WI for removing of masking to be made & displayed.Mukesh Kumar Singh06/04/202204/04/2022Completed
Outflow1-Awareness training to be provided to the final inspector.Sarvesh Kumar06/04/202205/04/2022Completed
Outflow100% visual inspection is started at M/s steel Engineers end with proper identification marking.Mukesh Kumar Singh06/04/202202/04/2022Completed
OutflowPowder coating defects matrix to be made & displayed at final inspection stage and training to be providedSunil04/04/202204/04/2022Completed
Occurance3-OJT to be provided for removing the masking.Mukesh Kumar Singh06/04/202205/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% visual inspection is started at M/s steel Engineers end with proper identification marking.
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Masking pull directly from the part before oven through hand
35_Occurance_Before.xlsx
Occurance (After) Method of removing the masking will be defined i.e masking will be removed through plastic stick.
35_Occurance_After.pdf
Outflow (Before) Not Available
35_Outflow_Before.pdf
Outflow (After) Powder coating defects matrix to be made & displayed at final inspection stage and training to be provided.
35_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL UBA
 
12. Document Review
Documents WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission OK