QFR No - 8000782618
Defect Details
NC No. 8000782618
NC Date 03/04/2022
NC Submission Date
Part No. S2HT52107B
Part Name OUTER SPRING K0PG
Supplier Name & Code 101048-STUMPP SCHUELE AND SOMAPPA SPR
ETL Plant 1136-ETL Suspension Sanand
Defect Details NOT AS PER SPECIFICATION-BEND FOUND AT CUSTOMER END DUE TO PARLL.
 
1. Problem Description
Defect Description Bend Found at Customer End due to Parallelism, Squarness NG i.e. Parallelism :- 1.66, 2.04, 2.41 Squarnes :- 7.5, 6.8, 8.0 it is repeatative at M/s ETLS end.
Detection Stage Customer End
Problem Severity Function
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID pathan.ak@ssssprings.com
Plant Head/CEO Email ID udham.singh@ssssprings.com
MD Email ID rln@ssssprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3080
0
0
0
700
3780
Check Qty
3080
0
0
0
700
3780
NG Qty
71
0
0
0
6
77
 
Scrap 77
Rework 0
Under Deviation 0
Containment Action
All the parts at Customer end inspected height gauge set up. 3080 parts checked and found 71 parts NG. Available internal parts segregated with Right angle and dial gauge set up. Available Qty of 700 nos. checked, 6 part found having ID undersize.
 
3. Process Flow
Process Flow Description
Recipt & inspection - Visual - Storage of material - Winding RH - Stress Relieving - Grinding - Shot peening - Scragging - Lo,OD,e1 & bend sorting and correction - Stress Relieving (LTA) - Powder coating - Final Inspection - Packing
 
4. Process Details
Process / Operation Grinding Operation
Outsource No
Machine / Cell SGM-3 / Halol
Machine / Cell No. Grinding Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineWrong end coil winding gap during coilingVerified and found the correct winding gap at coiling stageO
ManUnskilled OperatorSkilled operator deputed at each stageO
ToolWrong magazine plate / Bush size at Grinding stageVerified and found the magazine plate bush oversize by 1mm.X
MethodWrong orientation of spring in Grinding bush.Verified and found the spring orientation as defiened in work instruction (Bigger side upward)O
MethodInspection method errorVerified & found the base plate of the right angle block small in size, where some portion of the spX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Parts with parallelism more than 1mm produced at grinding stage.
Why 2 Grinding plate bush size observed 1mm more than specified. (Bush I.D observed 56.7mm against 55.7 mm max.
Why 3 Inspection frequency for Bush size I.D monitoring found less
Why 4
Why 5
Root Cause (Occurance) Inspection frequency for Bush size I.D monitoring found less
 
Root Cause Analysis (Outflow)
Why 1 Parallelism out of specification part escaped from inspection
Why 2 Dial gauge reading observed less with compare to readings at height gauge
Why 3 Verified & found the base plate of the right angle block small in size, where some portion of the spring base was resting outside of the base plate.
Why 4
Why 5
Root Cause (Outflow) Verified & found the base plate of the right angle block small in size, where some portion of the spring base was resting outside of the base plate.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew grinding plate with new Bushes with correct I.D produced and installed at Grinding stage.Mr. Dixit28/04/202228/04/2022Completed
OccuranceInspection frequency increased from 1 month to every set up of grinding. Control for Bush I.D monitoring added in Control plan.Mr. Maulesh28/04/202228/04/2022Completed
OutflowNew Right angle block with bigger Base plate introduced at inspection stage to avoid the inspection error.Mr. Maulesh21/04/202221/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection frequency increased from 1 month to every set up of grinding. Control for Bush I.D monitoring added in Control plan New Right angle block with bigger Base plate introduced at inspection stage to avoid the inspection error.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Inspection frequency for Bush size I.D monitoring found less. Grinding Bush I.D observed oversize
42_Occurance_Before.pdf
Occurance (After) Inspection frequency increased from 1 month to every set up of grinding. Control for Bush I.D monitoring added in Control plan. New Grinding plate with correct bush I.D produced and installed.
42_Occurance_After.pdf
Outflow (Before) Right angle block base was short, where some portion of the spring base falling out (of the base plate) during inspection.
42_Outflow_Before.jfif
Outflow (After) New Right angle block with bigger Base plate introduced at inspection stage to avoid the inspection error.
42_Outflow_After.jfif
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable for all the OC springs.
 
12. Document Review
Documents ControlPlan, PMCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission Accepted