QFR No - 8000782917
Defect Details
NC No. 8000782917
NC Date 06/04/2022
NC Submission Date
Part No. F1GN01102B
Part Name MAIN SPRING K86A
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1136-ETL Suspension Sanand
Defect Details HIGHT O/SIZE.-TOTAL HIGHT OVERSIZE
 
1. Problem Description
Defect Description Total Length Over Size
Detection Stage Inprocess
Problem Severity Function
NG Quantity 7
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID arun@helicalsprings.in
Plant Head/CEO Email ID Shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
0
0
0
8950
18950
Check Qty
10000
0
0
0
8950
18950
NG Qty
7
0
0
0
0
7
 
Scrap 7
Rework 0
Under Deviation 0
Containment Action
100% inspection done for length at ETL & Warehouse.
 
3. Process Flow
Process Flow Description
Raw Material Receipt & Inspection, Coiling, Stress Relieving, End Grinding, Shot Peening, Scragging, Length & Wavyness checking, Strain-aging, Surface Finish- Oiling, Final Inspection/ PDI, Packing, Dispatch.
 
4. Process Details
Process / Operation Coiling
Outsource No
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper material handingSetup part mix with ok partX
MaterialAs per DrawingRMTC checked found okO
MachineHerdonFound okO
ManUnskilled operatorSkill Matrix checked found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5 Nos
7. Root Cause Analysis (Occurance)
Why 1 length over size
Why 2 During setup length short spring coiled
Why 3 Setup quantity mix with the ok material
Why 4 No provision was available for setup part storage
Why 5
Root Cause (Occurance) Yellow bin introduced at coiling to keep suspected/setup part
 
Root Cause Analysis (Outflow)
Why 1 length over size
Why 2 Length gauge setting disturbed
Why 3 Improper locking of Length gauge
Why 4 No cross check method for length gauge verification
Why 5
Root Cause (Outflow) Dedicated length gauge will be introduced for K0LA main spring (fixed type)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowDedicated length gauge will be introduced for K0LA main spring (fixed type)Mr. Arun Kumar30/04/202228/04/2022Completed
Occurance1.Yellow bin introduced at coiling to keep suspected/setup part 2.OPL displayed at coiling 3.Training provided to the operator and recorded the sameMr. Nilesh Kapure14/04/202212/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Free length will be introduced for K0LA main spring (fixed type)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 30/Lot
10. Evidance of Countermeasure
Occurance (Before) No 100% marking on springs.
44_Occurance_Before.pdf
Occurance (After) 100% marking on spring After free length checking.
44_Occurance_After.pdf
Outflow (Before) Red bin & Yellow bin not cover properly.
44_Outflow_Before.pdf
Outflow (After) Red bin & Yellow bin cover properly
44_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Similar Part.
 
12. Document Review
Documents
Specify Other Document Opl
 
13. Effectiveness Of Action
Reviewed Quantity 12000
Reason for submission Found Ok