QFR No - 8000783094
Defect Details
NC No. 8000783094
NC Date 07/04/2022
NC Submission Date
Part No. F2DZ08810B
Part Name K0PG FORK BOLT
Supplier Name & Code 101037-SHREE PATEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details DEEP MARK-MACHINING UNCLEAN
 
1. Problem Description
Defect Description Line mark at OD 26.15
Detection Stage Inprocess
Problem Severity Function
NG Quantity 35
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality_spi@rediffmail.com
Plant Head/CEO Email ID planthead_spi@rediffmail.com
MD Email ID rspatel_spi@rediffmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
0
0
2618
0
12618
Check Qty
10000
0
0
2618
0
12618
NG Qty
1
0
0
2
0
3
 
Scrap 3
Rework 0
Under Deviation 0
Containment Action
Hold the material at all stages and inspection done accordingly .
 
3. Process Flow
Process Flow Description
1. Incoming RM 2. Acid Pickling 3. Water Wash 4. Lime Wash 5. Pointing 6. Draw 7. Cutting 8. Straightening 9. Inspection 10.Packing & Dispatch 11. Incoming RM 12. Traub Turning 13. CNC 1st set up 14. CNC 2nd set up 15. Plating 16. Inspection 17. Packing & Dispatch
 
4. Process Details
Process / Operation Draw
Outsource No
Machine / Cell Draw Machine
Machine / Cell No. Draw Line
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManAwareness of InspectorOperator was not aware about inspection stdO
MachineDie Check sheetDuring process Verification no Die check point availableO
MethodRod DrawDuring process verification a deep line mark generated on rod during draw operation.O
MachineDie Life MonitoringDuring process Verification no Die life monitoring record availableO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05
7. Root Cause Analysis (Occurance)
Why 1 Deep Line mark part reached at customer end.
Why 2 Deep line mark part generate during CNC operation.
Why 3 Deep line mark found on input rod .
Why 4 At draw operation chips observed on rod, which remains a deep line on rod during draw process.
Why 5 There was No checkpoint & WI available at draw operation to check the input & output material of rod.
Root Cause (Occurance) At draw operation chips observed on rod which generate / remains a deep line on rod during draw operat
 
Root Cause Analysis (Outflow)
Why 1 Deep Line mark part reached at customer end.
Why 2 Inspector not detected deep line mark part during final inspection .
Why 3 Inspector was not aware about the defect.
Why 4 No inspection std available at final inspection station.
Why 5
Root Cause (Outflow) No inspection std available at final inspection station.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. WI made to check the Input & Output material & also FIR ,IIR made to check the draw bar after draw process . 2. Draw Die checkpoint check sheet made . 3. Die life monitoring to be startedPradeep Tripathi18/02/202218/02/2022Completed
Outflow1. Training provided to the final inspector about the problem and inspection std. 2. 200% visual inspection started.Pradeep Tripathi18/02/202218/02/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 200% Visual Inspection
Inspection Method Other
Other Inspection Method Visual Inspection.
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Die Check Sheet
45_Occurance_Before.zip
Occurance (After) Die Check Sheet
45_Occurance_After.zip
Outflow (Before) Inspection Std
45_Outflow_Before.xlsx
Outflow (After) Inspection Std
45_Outflow_After.zip
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents ControlPlan, PMCheckSheet, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 0
Reason for submission Draw Die PM Sheet updated but revision number not changed. Also Document Control plan and PFMEA not updated as per revised Checking frequency and possible causes.