QFR No - 8000783465
Defect Details
NC No. 8000783465
NC Date 11/04/2022
NC Submission Date
Part No. 520AE00200
Part Name CORE PLATE K1 & K2
Supplier Name & Code 100959-AAR CEE ENGINEERING WORKS UNIT
ETL Plant 1135-ETL 7/10 P Nagar
Defect Details SURFACE FINISH NOT OK-RA VALUE LESS THAN 2RA
 
1. Problem Description
Defect Description Shot Blasting not done on one side of Plates. its Ra value observed as 1.38,1.36,1.39,1.42,1.48 against the minimum specification of 2 to 3 Ra
Detection Stage Receipt
Problem Severity Function
NG Quantity 32
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qc@aarceeengg.com
Plant Head/CEO Email ID planthead.diecasting@aarceeengg.com
MD Email ID vaibhav.arora@aarceeengg.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
0
0
2000
0
7000
Check Qty
5000
0
0
2000
0
7000
NG Qty
32
0
0
10
0
42
 
Scrap 0
Rework 42
Under Deviation 0
Containment Action
All materials are segregated at the customer end (ETL end) as well as supplier FG (AAR CEE end). NG pieces re-shot blasting to be done.
 
3. Process Flow
Process Flow Description
10. Receipt of Raw Material 20. Storage of Raw Material 30. Holding Cum Melting 40. PDC 50. Trimming 60. Shot Blasting 70. Barrelling 80. Sound Testing 90. Stress Relieving 100. Final Inspection & Packing 110. Storage & Dispatch
 
4. Process Details
Process / Operation 60. Shot Blasting
Outsource No
Machine / Cell Shot Blasting Machine
Machine / Cell No. SBM-02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineIn Shot Blasting Machine one side liner got broken suddenlyOne side liner found broken in Shot Blasting MachineX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 pieces
7. Root Cause Analysis (Occurance)
Why 1 Ra value found less than 2 Ra due to one side liner getting broken suddenly in the shot blasting machine.
Why 2 Operator not aware of such kind of issue
Why 3 The operator was not aware, there was no checkpoint on the check sheet for the shot blasting machine liner
Why 4
Why 5
Root Cause (Occurance) There was no checkpoint in the check sheet for the shot blasting machine liner.
 
Root Cause Analysis (Outflow)
Why 1 Ra value found less than 2 Ra due to Ra value check at two places of the core plate
Why 2 Quality Person not aware of the same
Why 3 There was no method defined to check the Ra value on the core plate
Why 4
Why 5
Root Cause (Outflow) There was no method defined to check the Ra value on the core plate
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCheck point for liner inspection to be added in check sheetAnkit Gupta21/04/202221/04/2022Completed
OutflowRa value checking method to be defined in control plan, PFEMA & inspection reportAnkit Gupta21/04/202221/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Ra value to be checked in process at 4 places of the core plate instead of 2 places
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 pieces
10. Evidance of Countermeasure
Occurance (Before) Check sheet before adding the checkpoint for liner
48_Occurance_Before.pdf
Occurance (After) Check sheet after adding the checkpoint for liner
48_Occurance_After.pdf
Outflow (Before) Inspection report before defining the method to check the Ra value
48_Outflow_Before.pdf
Outflow (After) Inspection report after defining the method to check the Ra value
48_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All model core plates
 
12. Document Review
Documents ControlPlan, PFMEA, JHCheckSheet, InspCheckSheet
Specify Other Document No other documents
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission ok