QFR No - 8000783854
Defect Details
NC No. | 8000783854 |
NC Date | 14/04/2022 |
NC Submission Date | |
Part No. | F2AV00902B |
Part Name | BELLOW -ABWB |
Supplier Name & Code | 101023-FORES ELASTOMECH INDIA PVT. LT |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-DAMAGED PARTS TORN BELLOW |
1. Problem Description
Defect Description | DIRT DAMAGES ON PLATE |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 82 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | malani.pritam@foresgroup.com |
Plant Head/CEO Email ID | singh.barinder@foresgroup.com |
MD Email ID | swamy.pj@foresgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
1000
|
0
|
2000
|
Check Qty |
1000
|
0
|
0
|
1000
|
0
|
2000
|
NG Qty |
2
|
0
|
0
|
0
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% stock verification at ETL end |
3. Process Flow
Process Flow Description |
---|
Rubber & Chemical >Incoming inspection > Mixing rubber compound > Moulding > Visual Inspection > Packing & Dispatch . |
4. Process Details
Process / Operation | Rubber Moulding |
Outsource | No |
Machine / Cell | Moulding |
Machine / Cell No. | Moulding |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Skip for inspection | Inspector not quarantine NG parts | O |
Machine | Mould temperature not okay | PLC controlled process parameter machine | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Flow mark on part |
Why 2 | Material Flow not uniform |
Why 3 | Dirt deposition in cavity |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Dirt deposition in cavity |
Root Cause Analysis (Outflow)
Why 1 | Material flow mark on part |
Why 2 | Skip from inspection |
Why 3 | Not okay material mix up in okay part |
Why 4 | inspector not quarantine NG parts |
Why 5 | |
Root Cause (Outflow) | Inspector not aware about the issue |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Dirt polishing frequency is increase | Fores | 19/04/2022 | 19/04/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No change |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Dirt polishing frequency is less i.e After 15days of production 51_Occurance_Before.png |
Occurance (After) |
1.Dirt polishing frequency is increase i.e After 7 days of production .
2.OPL display at production stage . 51_Occurance_After.png |
Outflow (Before) |
Inspector not aware about the issue 51_Outflow_Before.pdf |
Outflow (After) |
1.Training given to inspector .
2. OPL display at inspection stage . 51_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | N/A |
12. Document Review
Documents | |
Specify Other Document | N/A |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | Occurrence side & outflow side before after evidences are same. Also Horizontal deployment of action can be taken in FAV00302 which is not considered.(Same defect is repeating in F2AV00302) |