QFR No - 8000783854
Defect Details
NC No. 8000783854
NC Date 14/04/2022
NC Submission Date
Part No. F2AV00902B
Part Name BELLOW -ABWB
Supplier Name & Code 101023-FORES ELASTOMECH INDIA PVT. LT
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-DAMAGED PARTS TORN BELLOW
 
1. Problem Description
Defect Description DIRT DAMAGES ON PLATE
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 82
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID malani.pritam@foresgroup.com
Plant Head/CEO Email ID singh.barinder@foresgroup.com
MD Email ID swamy.pj@foresgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
1000
0
2000
Check Qty
1000
0
0
1000
0
2000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
100% stock verification at ETL end
 
3. Process Flow
Process Flow Description
Rubber & Chemical >Incoming inspection > Mixing rubber compound > Moulding > Visual Inspection > Packing & Dispatch .
 
4. Process Details
Process / Operation Rubber Moulding
Outsource No
Machine / Cell Moulding
Machine / Cell No. Moulding
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManSkip for inspectionInspector not quarantine NG partsO
MachineMould temperature not okayPLC controlled process parameter machineX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Flow mark on part
Why 2 Material Flow not uniform
Why 3 Dirt deposition in cavity
Why 4
Why 5
Root Cause (Occurance) Dirt deposition in cavity
 
Root Cause Analysis (Outflow)
Why 1 Material flow mark on part
Why 2 Skip from inspection
Why 3 Not okay material mix up in okay part
Why 4 inspector not quarantine NG parts
Why 5
Root Cause (Outflow) Inspector not aware about the issue
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDirt polishing frequency is increaseFores19/04/202219/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No change
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Dirt polishing frequency is less i.e After 15days of production
51_Occurance_Before.png
Occurance (After) 1.Dirt polishing frequency is increase i.e After 7 days of production . 2.OPL display at production stage .
51_Occurance_After.png
Outflow (Before) Inspector not aware about the issue
51_Outflow_Before.pdf
Outflow (After) 1.Training given to inspector . 2. OPL display at inspection stage .
51_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant N/A
 
12. Document Review
Documents
Specify Other Document N/A
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission Occurrence side & outflow side before after evidences are same. Also Horizontal deployment of action can be taken in FAV00302 which is not considered.(Same defect is repeating in F2AV00302)