QFR No - 8000783879
Defect Details
NC No. 8000783879
NC Date 14/04/2022
NC Submission Date
Part No. 580DL54702
Part Name FTL HUB CLUTCH VAVE 4 PLATE
Supplier Name & Code 205400-NAMO SAI INDUSTRIES
ETL Plant 1135-ETL 7/10 P Nagar
Defect Details BLOW HOLES-BLOW HOLE & OTHER CASTING DEFECTS
 
1. Problem Description
Defect Description Blow Holes & Multiple Pin Holes on the Insert Back face & in ID of Hub Vave, Rejection %age increased up to 29%, Till Date no rigid Action taken for the prevention & Reduction of same.
Detection Stage Inprocess
Problem Severity Function
NG Quantity 720
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID namosaiindustries@gmail.com
Plant Head/CEO Email ID namosaiindustries@gmail.com
MD Email ID mansingh@namosaiindustries.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
0
0
1000
400
2900
Check Qty
1500
0
0
1000
400
2900
NG Qty
720
0
0
10
0
730
 
Scrap 720
Rework 0
Under Deviation 0
Containment Action
100% Parts are check and putted the identification marks
 
3. Process Flow
Process Flow Description
PDC
 
4. Process Details
Process / Operation PDC
Outsource No
Machine / Cell PDC Machine
Machine / Cell No. PDC Machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine ParametersWater Pressure lessX
ToolProblem in Machine DieGasses not release properlyX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method No Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 1
7. Root Cause Analysis (Occurance)
Why 1 Below hole observed after machining
Why 2 Less water presser in die
Why 3 Less water pressure generate from pump
Why 4
Why 5
Root Cause (Occurance) Less water pressure generate from pump
 
Root Cause Analysis (Outflow)
Why 1 Below hole observed after machining
Why 2 Gasses not release during die casting
Why 3 No provision for gasses release in Die
Why 4
Why 5
Root Cause (Outflow) No provision for gasses release in Die
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceBooster pump added to increase the water pressureNamo Sai20/10/202220/10/2022Completed
OutflowOne Piece cut every one hrs to check the blow holeNamo Sai20/10/202220/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details One Piece cut every one hrs to check the blow hole
Inspection Method Other
Other Inspection Method Cut Piece Visual
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 1
10. Evidance of Countermeasure
Occurance (Before) Pump Before
53_Occurance_Before.jpg
Occurance (After) Pump After
53_Occurance_After.jpg
Outflow (Before) Die Before
53_Outflow_Before.jpg
Outflow (After) Die After
53_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All PDC Machine
 
12. Document Review
Documents ControlPlan
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission OK