QFR No - 8000783879
Defect Details
NC No. | 8000783879 |
NC Date | 14/04/2022 |
NC Submission Date | |
Part No. | 580DL54702 |
Part Name | FTL HUB CLUTCH VAVE 4 PLATE |
Supplier Name & Code | 205400-NAMO SAI INDUSTRIES |
ETL Plant | 1135-ETL 7/10 P Nagar |
Defect Details | BLOW HOLES-BLOW HOLE & OTHER CASTING DEFECTS |
1. Problem Description
Defect Description | Blow Holes & Multiple Pin Holes on the Insert Back face & in ID of Hub Vave, Rejection %age increased up to 29%, Till Date no rigid Action taken for the prevention & Reduction of same. |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 720 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | namosaiindustries@gmail.com |
Plant Head/CEO Email ID | namosaiindustries@gmail.com |
MD Email ID | mansingh@namosaiindustries.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
0
|
0
|
1000
|
400
|
2900
|
Check Qty |
1500
|
0
|
0
|
1000
|
400
|
2900
|
NG Qty |
720
|
0
|
0
|
10
|
0
|
730
|
Scrap | 720 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Parts are check and putted the identification marks |
3. Process Flow
Process Flow Description |
---|
PDC |
4. Process Details
Process / Operation | PDC |
Outsource | No |
Machine / Cell | PDC Machine |
Machine / Cell No. | PDC Machine |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Machine Parameters | Water Pressure less | X |
Tool | Problem in Machine Die | Gasses not release properly | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | No Method |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 1 |
7. Root Cause Analysis (Occurance)
Why 1 | Below hole observed after machining |
Why 2 | Less water presser in die |
Why 3 | Less water pressure generate from pump |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Less water pressure generate from pump |
Root Cause Analysis (Outflow)
Why 1 | Below hole observed after machining |
Why 2 | Gasses not release during die casting |
Why 3 | No provision for gasses release in Die |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No provision for gasses release in Die |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Booster pump added to increase the water pressure | Namo Sai | 20/10/2022 | 20/10/2022 | Completed |
Outflow | One Piece cut every one hrs to check the blow hole | Namo Sai | 20/10/2022 | 20/10/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | One Piece cut every one hrs to check the blow hole |
Inspection Method | Other |
Other Inspection Method | Cut Piece Visual |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 1 |
10. Evidance of Countermeasure
Occurance (Before) |
Pump Before 53_Occurance_Before.jpg |
Occurance (After) |
Pump After 53_Occurance_After.jpg |
Outflow (Before) |
Die Before 53_Outflow_Before.jpg |
Outflow (After) |
Die After 53_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All PDC Machine |
12. Document Review
Documents | ControlPlan |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 1 |
Reason for submission | OK |