QFR No - 8000784463
Defect Details
NC No. 8000784463
NC Date 20/04/2022
NC Submission Date
Part No. 53BHT00807
Part Name OUTER SPRING POWDER COATED-VAVE
Supplier Name & Code 101048-STUMPP SCHUELE AND SOMAPPA SPR
ETL Plant 1136-ETL Suspension Sanand
Defect Details PARALITY NOT OK.-BEND FOUND AT CUSTOMER END.
 
1. Problem Description
Defect Description Parallism More, Squarness More, Bend in Spring by Checking at Surface plate
Detection Stage Customer End
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID pathan.ak@ssssprings.com
Plant Head/CEO Email ID udham.singh@ssssprings.com
MD Email ID rln@ssssprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
0
0
0
0
1500
Check Qty
1500
0
0
0
0
1500
NG Qty
653
0
0
0
0
653
 
Scrap 572
Rework 81
Under Deviation 0
Containment Action
All the parts at Customer end inspected height gauge set up. 1500 parts checked and found 653 parts NG. No material was there in stock except at customer end.
 
3. Process Flow
Process Flow Description
Receipt & inspection - Visual - Storage of material - Winding RH - Stress Relieving - Grinding - Shot peening - Scragging - Lo,OD,e1 & bend sorting and correction - Powder coating - Final Inspection - Packing
 
4. Process Details
Process / Operation Grinding and inspection
Outsource No
Machine / Cell Grinding / Halol
Machine / Cell No. Grinding
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled OperatorSkilled operator deputed at coiling stageO
ToolWrong magazine plate / Bush size at Grinding stageVerified and found the magazine plate bush size correctO
MachineGrinding Surface Damage during grinding operationGrinding surface got damaged due to not changing the grinding wheel before life completionX
MethodWrong orientation of spring in Grinding bush.Verified and found the spring orientation as defined in work instruction (Bigger side upward)O
MethodInspection method errorVerified & found the base plate of the right angle block small in size, where some portion of the spX
MachineWrong end coil winding gap during coilingVerified and found the correct winding gap at coiling stageO
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Parts with parallelism more than specification produced at grinding stage.
Why 2 Grinding surface damage during grinding operation
Why 3 Grinding wheel damage
Why 4 Grinding wheel not replaced before life completion of Grinding wheel.
Why 5 Limit switch height to maintain grinding wheel thickness was not set at correct position
Root Cause (Occurance) Limit switch height to maintain grinding wheel thickness was not set at correct position
 
Root Cause Analysis (Outflow)
Why 1 Parallelism out of specification part escaped from inspection
Why 2 Dial gauge reading observed less with compare to readings at height gauge
Why 3 Verified & found the base plate of the right angle block small in size, where some portion of the spring base was resting outside of the base plate.
Why 4
Why 5
Root Cause (Outflow) Verified & found the base plate of the right angle block small in size, where some portion of the spring base was resting outside of the base plate.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceLimit Switch height to maintain grinding wheel thickness increased by 3mm so that grinding wheel can be disposed with minimum thickness of 15mm left. (To avoid overuse of grinding wheel, since the grinding wheel base is fit by 10mm bolts with the meatal gaurds & overuse of grinding wheel will cause spring getting struck with the bolts.) Validation performed and the limit switch height increased by 4mm found sufficient to maintain the correct grinding wheel thickness to avoid overuse of grinding wheel.Mr. Dixit28/04/202228/04/2022Completed
OutflowNew Right angle block with bigger Base plate introduced at inspection stage to avoid the inspection error.Mr. Maulesh21/04/202228/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details New Right angle block with bigger Base plate introduced at inspection stage to avoid the inspection error.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Grinding wheel height maintaining before the life completion was not getting monitored. Check point was not the part of Control plan.
59_Occurance_Before.pdf
Occurance (After) Limit Switch height to maintain grinding wheel thickness increased by 3mm so that grinding wheel can be disposed with minimum thickness of 15mm left. (To avoid overuse of grinding wheel, since the grinding wheel base is fit by 10mm bolts with the meatal guard & overuse of grinding wheel will cause spring getting struck with the bolts.) Control plan updated for the same.
59_Occurance_After.pdf
Outflow (Before) base plate of the right angle block small in size, where some portion of the spring base was resting outside of the base plate.
59_Outflow_Before.jfif
Outflow (After) New Right angle block with bigger Base plate introduced at inspection stage to avoid the inspection error.
59_Outflow_After.jfif
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Horizontally deployed for K0PG.
 
12. Document Review
Documents ControlPlan, PMCheckSheet, AuditCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission Accepted