QFR No - 8000785226
Defect Details
NC No. 8000785226
NC Date 25/04/2022
NC Submission Date
Part No. F2FA15933M
Part Name FORK PIPE MACHINED (K19 DRUM FF)
Supplier Name & Code 100634-TATA STEEL LIMITED
ETL Plant 1126-ETL Pantnagar
Defect Details CHAMFER NOT DONE-WRONG CHAMFER IDENTIFICATION -207 NOS.
 
1. Problem Description
Defect Description Ring mark/step over identification marking on K-19 fork pipe
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 207
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID bipldholpur@gmail.com
Plant Head/CEO Email ID anubhav.pandey@tatasteel.com
MD Email ID Praveens@tatasteel.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
500
500
0
0
0
1000
Check Qty
500
500
0
0
0
1000
NG Qty
207
60
0
0
0
267
 
Scrap 267
Rework 0
Under Deviation 0
Containment Action
Supply the next lot only after 100% inspection
 
3. Process Flow
Process Flow Description
CNC 1st setup (Threading) - 13x1.5° Chamfer Opertaion
 
4. Process Details
Process / Operation CNC Turning
Outsource No
Machine / Cell Macpower
Machine / Cell No. 3
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper chamfer or angle in dimension 13x1.5°In dimension 13x1.5°, ring mark/step up mark may generate at the end of chamfer due to lower angleX
ManUntrained Operator/InspectorOperator/Inspector not fully aware if this is visible after Grinding operationX
MaterialNo probable root cause related to materialInput material is as per specificationO
MachineNo probable root cause related to machineMachine operating as per given programO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Ring mark/step mark visible after grinding process
Why 2 Step mark generate during chamfer operation 13x1.5°
Why 3 Due to lower angle i.e. 1.5°
Why 4
Why 5
Root Cause (Occurance) Due to lower angle i.e. 1.5°
 
Root Cause Analysis (Outflow)
Why 1 Ring mark/step mark visible after grinding process
Why 2 Not detected during in-house inspection
Why 3 Not aware if this is visible after grinding process
Why 4
Why 5
Root Cause (Outflow) Not aware if this is visible after grinding process
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow100 % Visual inspection for Ring/step markPankaj29/05/202229/04/2022Completed
OccuranceAfter sample submission and further approval from ETL QA, dimension 13x1.5° changed to 13x1°55’Pankaj29/04/202229/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100%
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Dimension 13x1.5°
74_Occurance_Before.pdf
Occurance (After) Dimension 13x1°55`
74_Occurance_After.png
Outflow (Before) Inspection not done for Ring/Step mark
74_Outflow_Before.jpg
Outflow (After) 100 % Visual inspection for Ring/Step mark
74_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant K19 and K1 UG
 
12. Document Review
Documents Drawing
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission OK