QFR No - 8000785331
Defect Details
NC No. | 8000785331 |
NC Date | 26/04/2022 |
NC Submission Date | |
Part No. | 520FG00101 |
Part Name | HELICAL GEAR K-70 |
Supplier Name & Code | 100987-FLASH VIVEN MACHINING TECHNOLO |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | RUN OUT MORE-RUNOUT NOT OK,ID UNCLEAN |
1. Problem Description
Defect Description | Runout Excess Upto 0.6 mm as against 0.15 mm |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 160 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | sgn.quality@flashgroup.in |
Plant Head/CEO Email ID | dkj.mfg@flashgroup.in |
MD Email ID | sv.md@flashgroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3625
|
2000
|
2000
|
500
|
1500
|
9625
|
Check Qty |
3625
|
2000
|
2000
|
500
|
1500
|
9625
|
NG Qty |
81
|
0
|
0
|
12
|
23
|
116
|
Scrap | 81 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter. |
3. Process Flow
Process Flow Description |
---|
CNC-Hobbing-HT-Bore honning-teeth honning-Final inspection-dispatch |
4. Process Details
Process / Operation | HT |
Outsource | No |
Machine / Cell | heat treatment |
Machine / Cell No. | ht |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Warpage | Visual | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | Bend Near ID location |
Why 2 | Warpage near ID |
Why 3 | Resting on outer face in stack of 5 parts in HT charge |
Why 4 | No resting on counter face possibility of warpage |
Why 5 | No provision |
Root Cause (Occurance) | No resting on counter face possibility of warpage |
Root Cause Analysis (Outflow)
Why 1 | Skip at Final QA |
Why 2 | Sampling base inspection |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | 1) 100% Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter. 2) OPL & Q Alert Displayed |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1. To provide spacer in between two parts to such that gear rest on plane face 2. Lower end provide Square type spacer in between charge & part | AGD | 30/06/2022 | 30/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1) 100% Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter. 2) OPL & Q Alert Displayed |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
No resting on counter face possibility of warpage. 67_Occurance_Before.xlsx |
Occurance (After) |
To provide spacer in between two parts to such that gear rest on plane face
Lower end provide Square type spacer in between charge & part 67_Occurance_After.xlsx |
Outflow (Before) |
Sampling base inspection 67_Outflow_Before.xlsx |
Outflow (After) |
100% Visual & Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter. 67_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | JZ551400 & PF551402, DX551227 |
12. Document Review
Documents | WISOP |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | OK |