QFR No - 8000785331
Defect Details
NC No. 8000785331
NC Date 26/04/2022
NC Submission Date
Part No. 520FG00101
Part Name HELICAL GEAR K-70
Supplier Name & Code 100987-FLASH VIVEN MACHINING TECHNOLO
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details RUN OUT MORE-RUNOUT NOT OK,ID UNCLEAN
 
1. Problem Description
Defect Description Runout Excess Upto 0.6 mm as against 0.15 mm
Detection Stage Inprocess
Problem Severity Function
NG Quantity 160
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID sgn.quality@flashgroup.in
Plant Head/CEO Email ID dkj.mfg@flashgroup.in
MD Email ID sv.md@flashgroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3625
2000
2000
500
1500
9625
Check Qty
3625
2000
2000
500
1500
9625
NG Qty
81
0
0
12
23
116
 
Scrap 81
Rework 0
Under Deviation 0
Containment Action
100% Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter.
 
3. Process Flow
Process Flow Description
CNC-Hobbing-HT-Bore honning-teeth honning-Final inspection-dispatch
 
4. Process Details
Process / Operation HT
Outsource No
Machine / Cell heat treatment
Machine / Cell No. ht
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineWarpageVisualX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
7. Root Cause Analysis (Occurance)
Why 1 Bend Near ID location
Why 2 Warpage near ID
Why 3 Resting on outer face in stack of 5 parts in HT charge
Why 4 No resting on counter face possibility of warpage
Why 5 No provision
Root Cause (Occurance) No resting on counter face possibility of warpage
 
Root Cause Analysis (Outflow)
Why 1 Skip at Final QA
Why 2 Sampling base inspection
Why 3
Why 4
Why 5
Root Cause (Outflow) 1) 100% Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter. 2) OPL & Q Alert Displayed
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. To provide spacer in between two parts to such that gear rest on plane face 2. Lower end provide Square type spacer in between charge & partAGD30/06/202230/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1) 100% Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter. 2) OPL & Q Alert Displayed
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) No resting on counter face possibility of warpage.
67_Occurance_Before.xlsx
Occurance (After) To provide spacer in between two parts to such that gear rest on plane face Lower end provide Square type spacer in between charge & part
67_Occurance_After.xlsx
Outflow (Before) Sampling base inspection
67_Outflow_Before.xlsx
Outflow (After) 100% Visual & Flatness checking at Final inspection stage Next 5 lots with Blue dot marking near bore Diameter.
67_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant JZ551400 & PF551402, DX551227
 
12. Document Review
Documents WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK