QFR No - 8000785385
Defect Details
NC No. | 8000785385 |
NC Date | 26/04/2022 |
NC Submission Date | |
Part No. | 530CZ00102 |
Part Name | DU BUSH |
Supplier Name & Code | 100037-BBL DAIDO PRIVATE LIMITED |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | CHAMFER NOT DONE- WARRANTY ANALYSIS PART |
1. Problem Description
Defect Description | Uneven Chamfer and ID Coating Crumble observed in Warranty Return Parts, Also witnessed to supplier person. |
Detection Stage | Warranty |
Problem Severity | Function |
NG Quantity | 5 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | rajamani@bbldaido.com |
Plant Head/CEO Email ID | vinod@bbldaido.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5
|
0
|
0
|
0
|
0
|
5
|
Check Qty |
5
|
0
|
0
|
0
|
0
|
5
|
NG Qty |
5
|
0
|
0
|
0
|
0
|
5
|
Scrap | 5 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Bush investigated and found ID chamfer found OK and Bush material PTFE composition found good , hence Oil leak is not related to DU Bush. Available Bush at BBLD found OK |
3. Process Flow
Process Flow Description |
---|
RM Inspection - Slitting - Welding - Size rolling - Facing and chamfering -Pressing - Coining - Plating - Final Inspection - Despatch |
4. Process Details
Process / Operation | Facing and chamfering |
Outsource | No |
Machine / Cell | Bush Manufacturing line |
Machine / Cell No. | 5B-2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | ID Chamfer one side tool less depth of cut | Less depth of cut | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20 nos per |
7. Root Cause Analysis (Occurance)
Why 1 | ID Chamfer one side tool less depth of cut |
Why 2 | Coil Feed to chamfering tool contact space less |
Why 3 | Chamfer coil movement waviness not consider to run the parts maximum side |
Why 4 | Control dimension not provided in the process drawing |
Why 5 | |
Root Cause (Occurance) | Control dimension not provided in the process drawing |
Root Cause Analysis (Outflow)
Why 1 | Bush ID chamfer found NG |
Why 2 | Bush ID chamfer sampling ( 1 no per lot) inspection by contour |
Why 3 | Sampling not adequate to control the ID chamfer dimension |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Sampling not adequate to control the ID chamfer dimension |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1.Control dimension not provided in the process drawing | T.Rajamani | 05/05/2022 | 05/09/2022 | Completed |
Outflow | Visual inspection limit sample provided to check the less chamfer | T.Rajamani | 05/05/2022 | 05/09/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | ID chamfer band modified as per customer required chamfer |
Inspection Method | Other |
Other Inspection Method | ID chamfer provided |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20 |
10. Evidance of Countermeasure
Occurance (Before) |
Refer attached 77_Occurance_Before.pdf |
Occurance (After) |
Refer attached 77_Occurance_After.pdf |
Outflow (Before) |
Refer attached 77_Outflow_Before.pdf |
Outflow (After) |
Refer attached 77_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Not applicable |
12. Document Review
Documents | PFMEA, InspCheckSheet |
Specify Other Document | Process drawing |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |