QFR No - 8000785862
Defect Details
NC No. | 8000785862 |
NC Date | 30/04/2022 |
NC Submission Date | |
Part No. | 16JPP00117 |
Part Name | WHEEL CLUTCH REML 6 PLATE / 7 PLATE |
Supplier Name & Code | 100656-MADHURA DIE CAST PVT.LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | CRACK-LUG CRACK |
1. Problem Description
Defect Description | Crack |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 2 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | madhuradiecast@gmail.com |
Plant Head/CEO Email ID | madhuradiecast@gmail.com |
MD Email ID | madhuradiecast@gaikegroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
500
|
0
|
0
|
200
|
300
|
1000
|
Check Qty |
500
|
0
|
0
|
200
|
300
|
1000
|
NG Qty |
2
|
0
|
0
|
0
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Stock Segregation done at the Customer end, supplier end with blue dot marking on lug side. |
3. Process Flow
Process Flow Description |
---|
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection |
4. Process Details
Process / Operation | Casting |
Outsource | No |
Machine / Cell | PDC 400T |
Machine / Cell No. | 04 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskill Operator On machine. | Skill Matrix Varified & Found OK. | O |
Tool | Die Blue Matching not Done. | Found Not ok | X |
Machine | Water Was Leakage in Die | Checking water leakage & Found Ok. | O |
Material | Degassing was not done on decide frequency. | Melting cum furnace degassing report verified & found ok. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
7. Root Cause Analysis (Occurance)
Why 1 | Crack Observed on Lug |
Why 2 | Crack is Generated because of cold shot |
Why 3 | Die was Flashing |
Why 4 | Blue Matching not done |
Why 5 | |
Root Cause (Occurance) | Blue Matching not done |
Root Cause Analysis (Outflow)
Why 1 | Crack Observed on Lug |
Why 2 | NG Component Was mixed with ok component. |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | NG Component Was mixed with ok component. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 1 Tagging to all bin 2 Rejection and ok component area are define 3 Lock and key rejection bin wii be implement | Quality Superviser | 20/05/2022 | 11/07/2022 | Completed |
Occurance | 1 Die Blue matching done. 2 OPL Displayed on casting stage. | Production Superviser | 19/05/2022 | 18/07/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | This defect is monitoring on Q Gate. started 200% Inspection with identification marking |
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
10. Evidance of Countermeasure
Occurance (Before) |
Blue Matching not done 81_Occurance_Before.jpeg |
Occurance (After) |
1 Die Blue matching done. 2 OPL Displayed on casting stage. 81_Occurance_After.jpeg |
Outflow (Before) |
NG Component Was mixed with ok component. 81_Outflow_Before.jpeg |
Outflow (After) |
1 Tagging to all bin 2 Rejection and ok component area are define 3 Lock and key rejection bin wii be implement 81_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | no |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | QA OPL |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |