QFR No - 8000785862
Defect Details
NC No. 8000785862
NC Date 30/04/2022
NC Submission Date
Part No. 16JPP00117
Part Name WHEEL CLUTCH REML 6 PLATE / 7 PLATE
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details CRACK-LUG CRACK
 
1. Problem Description
Defect Description Crack
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
500
0
0
200
300
1000
Check Qty
500
0
0
200
300
1000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
100% Stock Segregation done at the Customer end, supplier end with blue dot marking on lug side.
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection
 
4. Process Details
Process / Operation Casting
Outsource No
Machine / Cell PDC 400T
Machine / Cell No. 04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskill Operator On machine.Skill Matrix Varified & Found OK.O
ToolDie Blue Matching not Done.Found Not okX
MachineWater Was Leakage in DieChecking water leakage & Found Ok.O
MaterialDegassing was not done on decide frequency.Melting cum furnace degassing report verified & found ok.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 Crack Observed on Lug
Why 2 Crack is Generated because of cold shot
Why 3 Die was Flashing
Why 4 Blue Matching not done
Why 5
Root Cause (Occurance) Blue Matching not done
 
Root Cause Analysis (Outflow)
Why 1 Crack Observed on Lug
Why 2 NG Component Was mixed with ok component.
Why 3
Why 4
Why 5
Root Cause (Outflow) NG Component Was mixed with ok component.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1 Tagging to all bin 2 Rejection and ok component area are define 3 Lock and key rejection bin wii be implementQuality Superviser20/05/202211/07/2022Completed
Occurance1 Die Blue matching done. 2 OPL Displayed on casting stage.Production Superviser19/05/202218/07/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details This defect is monitoring on Q Gate. started 200% Inspection with identification marking
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) Blue Matching not done
81_Occurance_Before.jpeg
Occurance (After) 1 Die Blue matching done. 2 OPL Displayed on casting stage.
81_Occurance_After.jpeg
Outflow (Before) NG Component Was mixed with ok component.
81_Outflow_Before.jpeg
Outflow (After) 1 Tagging to all bin 2 Rejection and ok component area are define 3 Lock and key rejection bin wii be implement
81_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant no
 
12. Document Review
Documents InspCheckSheet
Specify Other Document QA OPL
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission