QFR No - 8000786394
Defect Details
NC No. 8000786394
NC Date 05/05/2022
NC Submission Date
Part No. F2PH00902B
Part Name VALVE RETAINER (C101B)
Supplier Name & Code 101037-SHREE PATEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details NOT AS PER SPECIFICATION-CONCENTRICITY MORE (0.1)
 
1. Problem Description
Defect Description Concentricity found out of specification (0.19, 0.18, 0.22, 0.26 mm against the spec of 0.1mm Max) due to which Facing fitment problem i.e. Part not passing Matting Parts
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 2211
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality_spi@rediffmail.com
Plant Head/CEO Email ID planthead_spi@rediffmail.com
MD Email ID rspatel_spi@rediffmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
14000
0
0
6000
0
20000
Check Qty
14000
0
0
6000
0
20000
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Hold the material at final stage and segregation done accordingly.
 
3. Process Flow
Process Flow Description
10. Incoming RM 20. Parting 30. Facing and Chamfering 40. CNC ID turning & Facing 50. OD Grinding 60. Zink Plating 70. Inspection 80. Packing & Dispatch
 
4. Process Details
Process / Operation CNC ID turning & Facing
Outsource No
Machine / Cell CNC M/C
Machine / Cell No. M/C-10
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineClamping PressureDuring Gemba visit, clamping pressure of CNC m/c found inadequateX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05
7. Root Cause Analysis (Occurance)
Why 1 Concentricity found out of spec.
Why 2 Concentricity generate out of spec. during CNC process.
Why 3 Clamping pressure found inadequate during process.
Why 4 Operator was not aware about the Clamping pressure specification.
Why 5 No indication done on clamping pressure.
Root Cause (Occurance) 1. Clamping pressure found inadequate during process. 2. No indication done on clamping pressure
 
Root Cause Analysis (Outflow)
Why 1 Concentricity found out of spec.
Why 2 Parts were not traced in final inspection .
Why 3 Concentricity not checked during final inspection.
Why 4
Why 5
Root Cause (Outflow) Concentricity not checked during final inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceRed and Green indication Marking done on Clamping Pressure dial to easily understand to operators.Pradeep Tripathi16/05/202216/05/2022Completed
OutflowSampling inspection started for concentricity check.Pradeep Tripathi16/05/202216/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No Change
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05
10. Evidance of Countermeasure
Occurance (Before) CP
88_Occurance_Before.xlsx
Occurance (After) CP
88_Occurance_After.xlsx
Outflow (Before) Sampling Plan
88_Outflow_Before.xls
Outflow (After) Sampling Plan
88_Outflow_After.xls
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents ControlPlan
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Ok