QFR No - 8000786395
Defect Details
NC No. 8000786395
NC Date 05/05/2022
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details BUFFING DEFECT-BUFFING STEP, PLATING DEFECTS,
 
1. Problem Description
Defect Description Buffing Defects like Buffing Step, Buff Cut mark, Heavy Buffing Lines
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 105
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
1000
1000
1000
1000
5000
Check Qty
1000
1000
1000
1000
1000
5000
NG Qty
0
1
1
1
0
3
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
ALL MATERIAL SEGREGATED BT NICE STEEL IND.
 
3. Process Flow
Process Flow Description
10- BLANK 20- U BENDING 30- ROUNDING 40- WELDING 50- FLAIRING 60- ID SIZING 70 -SIDE(OD) GRINDING 80-BROACHING 90-HEAD GRINDING 100- PLATING(OUT SOURCE) 110-RECEIPT FROM PLATING 120-FINAL INSPECTION 130- PACKING & DISPATCH
 
4. Process Details
Process / Operation 70 -SIDE(OD) GRINDING
Outsource No
Machine / Cell 70 -SIDE(OD) GRINDING
Machine / Cell No. GRINDING
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWRONG MATERIAL USEDMATERIAL VERIFIED AND FOUND OKO
MachineMACHINE UNDER OR OVER CAPACITYMACHIN CAPACITY WAS OKO
ManUNTRAINED OPERATOROPREATOR WAS SKILLEDO
MethodUTTING FORCE WAS UNEVENWELDING BEAD NOT REMOVED IN UNIFORM SHAPEX
ToolWRONG BELT USEDBELT FOUND OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 STEP OBSERVED ON FACE OUTER DIA
Why 2 WELDING BEAD WAS NOT GRIND IN UNIFORM SHAPE
Why 3 WELDING BEAD NOT REMOVED PROPERLY
Why 4 CUTTING FORCE WAS NOT IN PROPER WAY
Why 5 OPERATOR NEGLIGENCE
Root Cause (Occurance) WELDING BEAD WAS NOT GRIND IN UNIFORM SHAPE
 
Root Cause Analysis (Outflow)
Why 1 STEP OBSERVED IN PARTS AT CUTOMER END
Why 2 PROBLEM COULD NOT FOUND DURING INSPECTION
Why 3 THIS PROBLEM WAS OBSERVED FIRST TIME
Why 4 SAMPLE WAS NOT AVAILABLE
Why 5
Root Cause (Outflow) THIS PROBLEM WAS OBSERVED FIRST TIME
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTRAINING PROVIDED TO OPREATOR FOR OD BUFFINGNICE STEEL IND10/05/202221/07/2022Completed
OutflowSAMPLE PROVIDED FOT VISUAL INSPECTIONNICE STEEL IND.10/05/202221/07/2022Completed
OutflowTRAINING PROVIDED TO ALL CONCERN PERSONNICE STEEL IND10/05/202221/07/2022Completed
OccuranceOPL DISPLAYED AT SHOP FLOOR FOR AWARENESSNICE STEEL IND10/05/202221/07/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% visual inspection started
Inspection Method Other
Other Inspection Method INSPECTOR DEFINED
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) NA
86_Occurance_Before.jpg
Occurance (After) 1-TRAINING PROVIDED TO ALL CONCERN PERSON 2- OPL DISPLAYED 3- SAMPLE PROVIDED
86_Occurance_After.pdf
Outflow (Before) NA
86_Outflow_Before.jpg
Outflow (After) 1-TRAINING PROVIDED TO ALL CONCERN PERSON 2- OPL DISPLAYED 3- SAMPLE PROVIDED
86_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL ADJUSTER
 
12. Document Review
Documents WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 7500
Reason for submission Found Ok in Reviewed Qty.