QFR No - 8000786469
Defect Details
NC No. | 8000786469 |
NC Date | 06/05/2022 |
NC Submission Date | |
Part No. | C2FY00233M |
Part Name | HUB CL. WITH INSERT MACHINED-D1 |
Supplier Name & Code | 100874-ANUSHRUSHTI AUTO PARTS |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | RUN OUT MORE-TEETH R/O O/S UP TO 0.40 MM |
1. Problem Description
Defect Description | Teeth OD Run out observed upto 0.4 mm as against 0.25 mm |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 25 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@anushrushtiautoparts.com |
Plant Head/CEO Email ID | anushrushti2011@rediffmail.com |
MD Email ID | rrwable@redffmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
300
|
0
|
0
|
0
|
0
|
300
|
Check Qty |
300
|
0
|
0
|
0
|
0
|
300
|
NG Qty |
25
|
0
|
0
|
0
|
0
|
25
|
Scrap | 25 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% inspection done for D1 HUB CL WITH INSERT with marking on TEETH. |
3. Process Flow
Process Flow Description |
---|
1.)RM INWARD 2) CNC 1ST SETUP 3) CNC 2ND SETUP 4) DRILLING 5)FINAL INSPECTION 6) PACKING & DISPATCH |
4. Process Details
Process / Operation | CASTING |
Outsource | Yes |
Machine / Cell | CNC 2 |
Machine / Cell No. | CNC 2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Inspector not aware of defect | Inspector skill matrix checked found ok | O |
Man | Operator not aware of defect | Operator training was not effective | X |
Method | Separate bins not used for storage | Operator is storing Parts in special partision bin | O |
Method | Part clamping & decampling not proper | uneven part clamping in jaw | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | MANDRELL& DIAL GAUGE |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5NO`S /LOT |
7. Root Cause Analysis (Occurance)
Why 1 | uneven part clamping in jaw |
Why 2 | heavy burr deposited at part clamping location (jaw) |
Why 3 | part clamping location not clean properly |
Why 4 | part clamping location cleaning frequency not define properly. |
Why 5 | |
Root Cause (Occurance) | part clamping location cleaning frequency not define properly. |
Root Cause Analysis (Outflow)
Why 1 | Part inspection frequency not evident |
Why 2 | Lot wise 5 no`s inspection fequency was define in control plan |
Why 3 | |
Why 4 | Part inspection frequency not evident |
Why 5 | |
Root Cause (Outflow) | Part inspection frequency not evident |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Partwise On job training are provided of all operator | Mr.Malhari pawar | 18/05/2022 | 18/05/2022 | Completed |
Outflow | Part inspection frequency not evident | Deepak singh | 27/05/2022 | 27/05/2022 | Completed |
Occurance | part clamping location cleaning frequency not define properly | malhari pawar | 16/06/2022 | 16/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1)Before - 5no`s per lot inspection done 2) After customer complaints -per bins 1 nos inspection started in final inspection |
Inspection Method | Other |
Other Inspection Method | dial+centerbetween |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | PER BINS 1 |
10. Evidance of Countermeasure
Occurance (Before) |
Jaw Burr cleaning frequency not define in control plan 95_Occurance_Before.xlsx |
Occurance (After) |
Jaw Burr cleaning define & updated in controlplan 95_Occurance_After.xlsx |
Outflow (Before) |
Face runout insp frequency was 5 no`s per lot 95_Outflow_Before.xlsx |
Outflow (After) |
Face runout insp frequency revied from 5 no`s per lot to 1 no`s per Bins 95_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Tranmission Division |
12. Document Review
Documents | ControlPlan |
Specify Other Document | On job training shee |
13. Effectiveness Of Action
Reviewed Quantity | 2000 |
Reason for submission | OK |