QFR No - 8000786759
Defect Details
NC No. 8000786759
NC Date 09/05/2022
NC Submission Date
Part No. F2BF26416M
Part Name OUTER TUBE BUFF LH K0NA DRUM
Supplier Name & Code 100001-ANANT ENTERPRISES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details THREADING NOT OK-M6 WITH OUT THREAD
 
1. Problem Description
Defect Description M6
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandkulkarni@anantgroup.co.in
Plant Head/CEO Email ID pramodgosavi@anantgroup.co.in
MD Email ID ashwinjoshi@anantgroup.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
2000
0
2000
Check Qty
0
0
0
2000
0
2000
NG Qty
0
0
0
1
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100 % segregation on inhouse stock & Dot identification on job.
 
3. Process Flow
Process Flow Description
Vmc 1st Setup Op-10
 
4. Process Details
Process / Operation Tapping operation
Outsource No
Machine / Cell vmc 1st setup op-10
Machine / Cell No. vmc 1st setup op-10
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineDue to abnormal situation tool brokenvisualO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 4
7. Root Cause Analysis (Occurance)
Why 1 M6 Tapping tool broken
Why 2 Due to abnormal situation in machine process
Why 3
Why 4
Why 5
Root Cause (Occurance) M6 tool broken due to abnormal situation in m/c process.
 
Root Cause Analysis (Outflow)
Why 1 No 100 % inspection for M6 TPG.
Why 2 Checking Frequency On Hourly Basis.
Why 3 No Awareness about this type of defect due to abnormal situation .
Why 4
Why 5
Root Cause (Outflow) No 100 % inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowQ-alert given to all operators & final inspectorsBhagyesh khairnar04/05/202204/05/2022Completed
OccuranceDefect CatLog updatedBhagyesh khairnar04/05/202204/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Dot identification at M6 lug Area.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) Training record
101_Occurance_Before.pdf
Occurance (After) Q Alert given to all operators & final inspector
101_Occurance_After.pdf
Outflow (Before) Identification mark on job
101_Outflow_Before.pdf
Outflow (After) Defect CatLog
101_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Kola Disc Bottom Case
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document Training record
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission