QFR No - 8000786759
Defect Details
NC No. | 8000786759 |
NC Date | 09/05/2022 |
NC Submission Date | |
Part No. | F2BF26416M |
Part Name | OUTER TUBE BUFF LH K0NA DRUM |
Supplier Name & Code | 100001-ANANT ENTERPRISES |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | THREADING NOT OK-M6 WITH OUT THREAD |
1. Problem Description
Defect Description | M6 |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 4 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandkulkarni@anantgroup.co.in |
Plant Head/CEO Email ID | pramodgosavi@anantgroup.co.in |
MD Email ID | ashwinjoshi@anantgroup.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
0
|
0
|
2000
|
0
|
2000
|
Check Qty |
0
|
0
|
0
|
2000
|
0
|
2000
|
NG Qty |
0
|
0
|
0
|
1
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % segregation on inhouse stock & Dot identification on job. |
3. Process Flow
Process Flow Description |
---|
Vmc 1st Setup Op-10 |
4. Process Details
Process / Operation | Tapping operation |
Outsource | No |
Machine / Cell | vmc 1st setup op-10 |
Machine / Cell No. | vmc 1st setup op-10 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Due to abnormal situation tool broken | visual | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 4 |
7. Root Cause Analysis (Occurance)
Why 1 | M6 Tapping tool broken |
Why 2 | Due to abnormal situation in machine process |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | M6 tool broken due to abnormal situation in m/c process. |
Root Cause Analysis (Outflow)
Why 1 | No 100 % inspection for M6 TPG. |
Why 2 | Checking Frequency On Hourly Basis. |
Why 3 | No Awareness about this type of defect due to abnormal situation . |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No 100 % inspection. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Q-alert given to all operators & final inspectors | Bhagyesh khairnar | 04/05/2022 | 04/05/2022 | Completed |
Occurance | Defect CatLog updated | Bhagyesh khairnar | 04/05/2022 | 04/05/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Dot identification at M6 lug Area. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
Training record 101_Occurance_Before.pdf |
Occurance (After) |
Q Alert given to all operators & final inspector 101_Occurance_After.pdf |
Outflow (Before) |
Identification mark on job 101_Outflow_Before.pdf |
Outflow (After) |
Defect CatLog 101_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Kola Disc Bottom Case |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | Training record |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |