QFR No - 8000787195
Defect Details
NC No. | 8000787195 |
NC Date | 11/05/2022 |
NC Submission Date | |
Part No. | 16JPP00117 |
Part Name | WHEEL CLUTCH REML 6 PLATE / 7 PLATE |
Supplier Name & Code | 100656-MADHURA DIE CAST PVT.LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | THREADING MISSING-THREADING MISSING & O/S ISSUE |
1. Problem Description
Defect Description | Thread missing to all six lugs |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 2 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | madhuradiecast@gmail.com |
Plant Head/CEO Email ID | madhuradiecast@gmail.com |
MD Email ID | madhuradiecast@gaikegroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
800
|
0
|
0
|
550
|
330
|
1680
|
Check Qty |
800
|
0
|
0
|
550
|
330
|
1680
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
1.100% All material segregation at customer end and inhouse end with identification blue marking on the lug. 2. Started operator traceability by initial of operator name mentioned on the component. |
3. Process Flow
Process Flow Description |
---|
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.VMC (6 Hole drilling and tapping) 6.Final Inspection |
4. Process Details
Process / Operation | VMC (6 Hole drilling and tapping) |
Outsource | No |
Machine / Cell | VMC |
Machine / Cell No. | VMC NO.01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Input & output material bin not identified on drilling tapping stage | Drilling tapping stage checked found not ok | X |
Man | Unskill operator operate machine | Skill matrix verify found ok | O |
Machine | Component was Rest wrong position | fixture checked not possiblity to rest wrongly | O |
Tool | Wrong grade drill and tapp used for operation | Checked and verify found ok | O |
Material | Double drilling and tapping done on component | Component checked found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10/Hr |
7. Root Cause Analysis (Occurance)
Why 1 | Threading missing -Threading missing and O/s. |
Why 2 | Drilling and tapping was not done on component. |
Why 3 | Without drilling and tapping component mix with ok components. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Without drilling and tapping component mix with ok components. |
Root Cause Analysis (Outflow)
Why 1 | Threading missing -Threading missing and O/s. |
Why 2 | TPG Checking done was sampling basis. |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | TPG Checking done was sampling basis. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1. Input material and output material Bin identified. 2. We change final inspection table location from away drilling tapping operation. 3. Started operator traceability by initial name mentioned on component & marking on Lug conformation of Threading operation done | Production Supervisor | 14/05/2022 | 12/05/2022 | Completed |
Outflow | 1. Started 100% Thread plug gauging checking and marking on the lug for gauging conformation. 2.QA alert & OPL , Displayed on final inspection table. 3. Defective sample displayed at final inspection table. | QA Supervisior | 12/05/2022 | 12/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Started 100% Thread plug gauging checking. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
10. Evidance of Countermeasure
Occurance (Before) |
Without drilling and tapping component mix with ok components.2. Input material and output material Bin not identified. 111_Occurance_Before.jpeg |
Occurance (After) |
1. Input material and output material Bin identified. 2. We change final inspection table location from away drilling tapping operation. 3. Started operator traceability by initial name mentioned on component & marking on Lug conformation of Threading operation done 111_Occurance_After.pdf |
Outflow (Before) |
TPG Checking done was sampling basis. 111_Outflow_Before.jpeg |
Outflow (After) |
1. Started 100% Thread plug gauging checking and marking on the lug for gauging conformation. 2.QA alert & OPL , Displayed on final inspection table. 3. Defective sample displayed at final inspection table. 111_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | Q-Alert,OPL |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | Analysis not proper -Input output material handling system should specify with color ,bins / trolleys type etc. for easily distinguish the parts |