QFR No - 8000787195
Defect Details
NC No. 8000787195
NC Date 11/05/2022
NC Submission Date
Part No. 16JPP00117
Part Name WHEEL CLUTCH REML 6 PLATE / 7 PLATE
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details THREADING MISSING-THREADING MISSING & O/S ISSUE
 
1. Problem Description
Defect Description Thread missing to all six lugs
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
800
0
0
550
330
1680
Check Qty
800
0
0
550
330
1680
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
1.100% All material segregation at customer end and inhouse end with identification blue marking on the lug. 2. Started operator traceability by initial of operator name mentioned on the component.
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.VMC (6 Hole drilling and tapping) 6.Final Inspection
 
4. Process Details
Process / Operation VMC (6 Hole drilling and tapping)
Outsource No
Machine / Cell VMC
Machine / Cell No. VMC NO.01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodInput & output material bin not identified on drilling tapping stageDrilling tapping stage checked found not okX
ManUnskill operator operate machineSkill matrix verify found okO
MachineComponent was Rest wrong positionfixture checked not possiblity to rest wronglyO
ToolWrong grade drill and tapp used for operationChecked and verify found okO
MaterialDouble drilling and tapping done on componentComponent checked found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10/Hr
7. Root Cause Analysis (Occurance)
Why 1 Threading missing -Threading missing and O/s.
Why 2 Drilling and tapping was not done on component.
Why 3 Without drilling and tapping component mix with ok components.
Why 4
Why 5
Root Cause (Occurance) Without drilling and tapping component mix with ok components.
 
Root Cause Analysis (Outflow)
Why 1 Threading missing -Threading missing and O/s.
Why 2 TPG Checking done was sampling basis.
Why 3
Why 4
Why 5
Root Cause (Outflow) TPG Checking done was sampling basis.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Input material and output material Bin identified. 2. We change final inspection table location from away drilling tapping operation. 3. Started operator traceability by initial name mentioned on component & marking on Lug conformation of Threading operation doneProduction Supervisor14/05/202212/05/2022Completed
Outflow1. Started 100% Thread plug gauging checking and marking on the lug for gauging conformation. 2.QA alert & OPL , Displayed on final inspection table. 3. Defective sample displayed at final inspection table.QA Supervisior12/05/202212/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Started 100% Thread plug gauging checking.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) Without drilling and tapping component mix with ok components.2. Input material and output material Bin not identified.
111_Occurance_Before.jpeg
Occurance (After) 1. Input material and output material Bin identified. 2. We change final inspection table location from away drilling tapping operation. 3. Started operator traceability by initial name mentioned on component & marking on Lug conformation of Threading operation done
111_Occurance_After.pdf
Outflow (Before) TPG Checking done was sampling basis.
111_Outflow_Before.jpeg
Outflow (After) 1. Started 100% Thread plug gauging checking and marking on the lug for gauging conformation. 2.QA alert & OPL , Displayed on final inspection table. 3. Defective sample displayed at final inspection table.
111_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO
 
12. Document Review
Documents InspCheckSheet
Specify Other Document Q-Alert,OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Analysis not proper -Input output material handling system should specify with color ,bins / trolleys type etc. for easily distinguish the parts