QFR No - 8000787245
Defect Details
NC No. 8000787245
NC Date 12/05/2022
NC Submission Date
Part No. 520FZ01002
Part Name HUB CLUTCH WITH INNER RING REML 6/7 PL
Supplier Name & Code 101100-CAST 4 ALUMINIUM PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details FITTMENT NOT OK.-Inner Ring Loose
 
1. Problem Description
Defect Description Inner ring loose
Detection Stage Warranty
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID info@cast4aluminium.com
Plant Head/CEO Email ID info@cast4aluminium.com
MD Email ID kiran@cast4aluminium.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1
0
0
0
0
1
Check Qty
1
0
0
0
0
1
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
RM INWARD - MELTING - CASTING - GATE CUTTING & FETTLING - IN PROCESS INSPECTION - CNC MACHINING - RING PRESSING - BROACHING - OD GRINDING - FINAL INSPECTION - DISPATCH
 
3. Process Flow
Process Flow Description
RE-CHECK ALL PIPE LINE MATERIAL.
 
4. Process Details
Process / Operation RING PRESSING
Outsource Yes
Machine / Cell PNEUMATIC PRESS MACHINE
Machine / Cell No. PRESS MACHINE - 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodCheck point for bolt tight/loose in PM check sheet.Observed no check point in PM check sheet.X
MachineScaling not available for bolt setting of sensorObserved no scaling on machine to set bolt.X
MaterialRing ID not as per specificationObserved ring oversize.X
 
6. Inspection Method Analysis (Current)
Inspection Method Pokayoke
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 NOS
7. Root Cause Analysis (Occurance)
Why 1 Ring not pressed properly due to pressing loader setting disturbed.
Why 2 Loader was shifted from the sensor face due to loose bolting.
Why 3 Pressing loader travelling length gets disturb due to bolt loose tightening.
Why 4 Scaling was not available to set bolt of sensor on machine.
Why 5 No check point for bolt loose/tight in PM check sheet.
Root Cause (Occurance) Scaling not available for bolt setting of sensor.
 
Root Cause Analysis (Outflow)
Why 1 Inspector not able to judge loose ring press operation.
Why 2 Part not detected in process validation.
Why 3 Ring ID inspection was on sample basis 5 nos/lot.
Why 4
Why 5
Root Cause (Outflow) Ring ID inspection was on sample basis 5 nos/lot
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1) Scaling provide to sensor setting on machine. 2) Check point added in PM check sheet and is monitored on daily basis. 3) Red colour coding implemented on setting piece rejection material.Mr. Deepak Singh17/05/202217/05/2022Completed
Outflow1) Process validation done on daily basis. 2) 100% inspection for ring ID on air ring gauge. 3) Q-Alert displayed. 4) Training given to inspector and operatorMr. Deepak Singh17/05/202217/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection for ring ID at inward inspection stage.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No scaling on machine to set sensor.
112_Occurance_Before.png
Occurance (After) Scaling provided to set sensor.
112_Occurance_After.png
Outflow (Before) Process validation report.
112_Outflow_Before.jpg
Outflow (After) Air gauge to inspect 100% at inward inspection stage.
112_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Not applicable.
 
12. Document Review
Documents PMCheckSheet, PokayokeCheckSheet, InspCheckSheet
Specify Other Document Inward check sheet.
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission ok