QFR No - 8000787544
Defect Details
NC No. | 8000787544 |
NC Date | 14/05/2022 |
NC Submission Date | |
Part No. | 520KS00102 |
Part Name | RIVET BR 100 CLUTCH |
Supplier Name & Code | 100049-METAFORGE ENGG.(I) PVT.LTD. |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | CRACK-HEAD CRACK |
1. Problem Description
Defect Description | Head Crack |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 110 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qa@metaforgeindia.com |
Plant Head/CEO Email ID | kaustubh@metaforgeindia.com |
MD Email ID | prajakt@metaforgeindia.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
9000
|
0
|
0
|
0
|
0
|
9000
|
Check Qty |
9000
|
0
|
0
|
0
|
0
|
9000
|
NG Qty |
9000
|
0
|
0
|
0
|
0
|
9000
|
Scrap | 0 |
Rework | 9000 |
Under Deviation | 0 |
Containment Action |
---|
VIsual inspection- In sampling |
3. Process Flow
Process Flow Description |
---|
Forging-Annealing- |
4. Process Details
Process / Operation | Forging |
Outsource | No |
Machine / Cell | Forging |
Machine / Cell No. | Forging |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Line marks on wire coil | Line mark shankand head | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | - |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | Head found crack |
Why 2 | During Head forging upsetting head found crack |
Why 3 | Line mark on RM coil surface are on some portion |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Line mark on RM coil surface are on some portion |
Root Cause Analysis (Outflow)
Why 1 | head found crack |
Why 2 | Not detect in visual inspection |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Not detect in visual inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Not defined | Adarsh | 15/06/2022 | 20/07/2022 | Completed |
Outflow | Vision base system ( proposal sent to ETL) | Adarsh | 15/06/2022 | 31/03/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | 0 |
Inspection Method | Other |
Other Inspection Method | - |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
- 118_Occurance_Before.pdf |
Occurance (After) |
- 118_Occurance_After.pdf |
Outflow (Before) |
- 118_Outflow_Before.pdf |
Outflow (After) |
- 118_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All rivet family |
12. Document Review
Documents | |
Specify Other Document | - |
13. Effectiveness Of Action
Reviewed Quantity | 50000 |
Reason for submission | 1.OK-No Repetition of Defect Phenomenon (Outflow side action OK) 2.Occurrence Side action to be submit |