QFR No - 8000787717
Defect Details
NC No. 8000787717
NC Date 17/05/2022
NC Submission Date
Part No. F1LG00902B
Part Name SEAT PIPE -K86A
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1146-ETL Suspension Narasapura
Defect Details HIGHT U/SIZE.-TOTAL LENGTH LESS ISSUE
 
1. Problem Description
Defect Description K0LA seat pipe total length less issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo nqppngc1jzrocztqb5vn0rur.xlsx
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
15000
0
0
7000
0
22000
Check Qty
15000
0
0
0
0
15000
NG Qty
4
0
0
0
0
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
Segregated all the material at ETL.
 
3. Process Flow
Process Flow Description
1.RM Receipt 2. Cutting 3.Multistation Draw 4. Head Formation 5. Rough Grinding 6. Punching 7. CNC Head Turning & Chamfering 8. CNC Boring & Facing 9. Thread M8x1.25 Tapping 10. Chamfering-1 11. Chamfering-2 12. ID Deburring 13. Finish Grinding 14. Final Inspection 15. ID Cleaning 16. Oiling 17. Packing & Dispatch.
 
4. Process Details
Process / Operation CNC Boring & Facing
Outsource No
Machine / Cell CNC
Machine / Cell No. NP/CNC/014
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator Negligence.Operator found to be non-negligent.O
ManOperator Unaware.Operator found to be aware about the Operation.O
MaterialMaterial Hardness Less/More.Material Hardness found to be ok.O
MethodNG setting part mixed.No locked Red Bin present at work station.X
MaterialOther model mixed during processing.Verified found OK .O
MethodCNC vernier not calibrated.Calibration certificateO
MethodUsage of open Red Bins.During Gemba visit open Red Bins observed to be present at work station.X
MethodCNC Stopper design inadequate.Verified found OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Asper plan
7. Root Cause Analysis (Occurance)
Why 1 Total length undersize.
Why 2 NG Setting part with length undersize passed.
Why 3 NG Setting part mixed in OK parts.
Why 4 Usage of open Red Bins.
Why 5
Root Cause (Occurance) Usage of open Red Bins.
 
Root Cause Analysis (Outflow)
Why 1 Total Length undersize.
Why 2 Could not be detected at Final Inspection.
Why 3 Skipped in Sampling at Final Inspection.
Why 4
Why 5
Root Cause (Outflow) Skipped in Sampling at Final Inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceLock & Key type rejection bins to be implemented at work station (Only part drop down and not pick up from Bin).Mr Mohinderpal26/05/2022Completed
OccuranceQuality Alert to be displayed at work station.Mr Lokesh20/05/2022Completed
OutflowQuality alert to be displayed at final inspectionMr. Lokesh20/05/2022Completed
OutflowSampling plan to be doubled at final inspection.Mr. Gurpreet23/05/2022Completed
OccuranceSetting NG part to be damaged by shift supervisor.Mr Lokesh27/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling to be doubled.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size doubled
10. Evidance of Countermeasure
Occurance (Before) Usage of open Red Bin.
126_Occurance_Before.jpg
Occurance (After) Lock & Key type rejection bins to be implemented.
126_Occurance_After.jpg
Outflow (Before) As per Sampling plan.
126_Outflow_Before.jpg
Outflow (After) Sampling doubled.
126_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All similar models.
 
12. Document Review
Documents WISOP
Specify Other Document No.
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission reviewed 5000 number no issue found ok