QFR No - 8000787777
Defect Details
NC No. | 8000787777 |
NC Date | 17/05/2022 |
NC Submission Date | |
Part No. | F2BF05707M |
Part Name | OUTER TUBE P/C RH (HMS-30) |
Supplier Name & Code | 101219-ROCKMAN INDUSTRIES |
ETL Plant | 1143-ETL Suspension Halol, Vadodara |
Defect Details | THREADING MISSING-HALF THREAD OBSERVED IN FENDER HOLE |
1. Problem Description
Defect Description | M6 Thread missing in fender hole |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | 0odo1tillahsmzo20nbc3tx5.jpg |
Supplier Communication Details
Quality Head Email ID | shriknat.sharma@rockman.in |
Plant Head/CEO Email ID | mlshah@rockman.in |
MD Email ID | skmishra2@rockman.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
500
|
0
|
0
|
500
|
0
|
1000
|
Check Qty |
500
|
0
|
0
|
500
|
0
|
1000
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Immediately segregate all the stock at M/s Endurance end and M/s Rockman end also , |
3. Process Flow
Process Flow Description |
---|
Casting - Gate Cutting /Buffing - Machining - Buffing - Leakage testing - washing - Inspection - Painting - Inspection and dispatch |
4. Process Details
Process / Operation | Machining process |
Outsource | No |
Machine / Cell | machining cell |
Machine / Cell No. | 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | dedicated machine are not in used | verified and found dedicated machined are being used fro the part | O |
Method | Pat wrong load in the machine | part loading in OK condition | O |
Material | wrong material used during casting | verified and found OK | O |
Man | New manpower deoute | Skilled manpower used on the machining center | O |
Tool | tool become worn out | verified and found tool become worn out | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
7. Root Cause Analysis (Occurance)
Why 1 | Drill Length Less. |
Why 2 | Home position missed by machine |
Why 3 | Home position memory forget after some time |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Home Position forget after some time |
Root Cause Analysis (Outflow)
Why 1 | Part skipped from final Inspection |
Why 2 | check point not given to Operator |
Why 3 | earlier there is no any check point added in the system |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | earlier there is no any check point added in the system |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Tapping Check as per sampling Plan Hourly monitoring at generation stage | Production | 16/06/2022 | 15/06/2022 | Completed |
Occurance | Machine CMOS changed | lalit | 16/06/2022 | 15/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Hourly monitoring started at machine shop |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
not applicable 122_Occurance_Before.pdf |
Occurance (After) |
not available 122_Occurance_After.pdf |
Outflow (Before) |
not applicable 122_Outflow_Before.pdf |
Outflow (After) |
Photo attached 122_Outflow_After.bmp |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | CMOS changed on all the machine |
12. Document Review
Documents | |
Specify Other Document | no change |
13. Effectiveness Of Action
Reviewed Quantity | 200 |
Reason for submission | Repeated issue observed in every month |