QFR No - 8000788016
Defect Details
NC No. 8000788016
NC Date 19/05/2022
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details NOT AS PER SPECIFICATION-MACHINING OPERATION(46.1+01MM DEPTH MISS
 
1. Problem Description
Defect Description Caulking Side (46.1 +0.1 mm Depth) Machining Operation Miss.
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID vijayakumarv@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2010
0
0
1500
700
4210
Check Qty
2010
0
0
1500
700
4210
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
1.100% Inspection Done at ETL end for all available Qty. 2.100% visual Inspection done for all available Qty of Machined Tubes KOPG & K86 - A Model with Blue Marking at Tube ID Chamfer at TI Sanand WH.
 
3. Process Flow
Process Flow Description
Incoming Material - Inward Inspection - Storage - CNC Machining Clip Side - CNC Machining Caulking Side - Drilling - Deburring - Final Inspection - Packing in Bins - Dispatch to ETL.
 
4. Process Details
Process / Operation CNC Machining Caulking Side
Outsource No
Machine / Cell CNC Machining Cell
Machine / Cell No. ACE CNC -02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodWrong SetupVerified through Gemba observation and found M/c Setup Repot OK.O
MachineMachining ParameterVerified through Gemba observation and found all Machine Parameter as per Control PlanO
MethodIncomplete M/C CycleVerified through Gemba observation and found that if Sudden power Failure / Sudden Emergency ButtonX
MachineSudden Machine BreakdownVerified through Gemba &facts found ACE CNC -02 M/c Stop frequently with error cabinet temp too highX
ManInspection SOP not Followedin Deburring Fixture Pokayoke , fully Inserted & rest at bottom Plate is not easily to visualize.X
 
6. Inspection Method Analysis (Current)
Inspection Method Pokayoke
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20 Nos/lot
7. Root Cause Analysis (Occurance)
Why 1 Caulking Depth of Dim. 46.10 +.10 mm Miss part found at Customer end.
Why 2 Incomplete Machining cycle
Why 3 ACE CNC -02 Machine Stopping in Running operation
Why 4 ACE CNC -02 m/c stopping with error cabinet temp too high.
Why 5 In ACE CNC -02 Machine Setting ( Handy ) value of Parameter write is wrong ( set by Manufacturer )
Root Cause (Occurance) In ACE CNC -02 Machine Setting ( Handy ) value of Parameter write is wrong ( set by Manufacturer )
 
Root Cause Analysis (Outflow)
Why 1 Caulking Depth of Dim. 46.10 +.10 mm Miss part found at Customer end.
Why 2 Part not Capture in De- Burring Fixture Poka-yoke ( at Bottom Side Bush Provided with OD 26 mm & Height 45 mm.)
Why 3 Operator not judged Part is fully Inserted & rest at bottom of Deburring Poka-yoke Fixture.
Why 4 Deburring Fixture poka-yoke Table Height is Less (380 mm ) & Burr Collecting box height ( 285 mm ) is More.
Why 5
Root Cause (Outflow) Deburring Fixture poka-yoke Table Height is Less (380 mm ) & Burr Collecting box height ( 285 mm ) is More.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAfter Discussion with ACE CNC M/C representative in Machine Setting ( Handy ) value of Parameter write changed from 1 to 0Mr. Bhupender Paji23/05/202222/05/2022Completed
OutflowTraining given to operator to check for Power Failure / Sudden stop of machine during operation part 100% for all Dimension and if part is not as per specification then the reject part.Mr. Bhupendra.20/09/202220/09/2022Completed
OutflowDeburring Poka-yoke Fixture table Height will Increase to 4 feet & Burr Collecting box height reduced to 50 mmMr. Palak Shah27/05/202226/05/2022Completed
OutflowDeburring Work Instruction Updated for tube should be rested fully to bottom.Mr.Piyush Parmar24/09/202223/09/2022Completed
OutflowOne Point Lesson Displayed at Deburring StationMr. Piyush Parmar24/09/202223/09/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Added Visual Check for Operation Miss with Identification marking in Caulking ID.
Inspection Method Other
Other Inspection Method Visual Insp.
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) In ACE CNC -02 Machine Setting ( Handy ) value of Parameter write is 1 due to this Machine stop in running with showing error of cabinet temp too high.
135_Occurance_Before.pdf
Occurance (After) To overcome the issue of cabinet temp too high resulting in machine Stoppage in Running in Machine Setting ( Handy ) value of Parameter write changed from 1 to 0
135_Occurance_After.pptx
Outflow (Before) Operator not able detected that Part is fully Inserted & rest at bottom of Deburring Poka- Yoke Fixture Cause of Deburring Fixture Table Height is Less (380 mm ) & Burr Collecting box height ( 285 mm ) is More.
135_Outflow_Before.pptx
Outflow (After) Deburring Poka-yoke Fixture table Height will Increase to 4 feet & Burr Collecting box height reduced to 50 mm . So Operator will easily detect that Part is fully Inserted & rest at bottom of Deburring Poka-yoke Fixture.
135_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ACE CNC -01 Machine TFF Tube Model - K86 -A
 
12. Document Review
Documents WISOP
Specify Other Document one Point Lesson
 
13. Effectiveness Of Action
Reviewed Quantity 14000
Reason for submission Operation miss part not reported again in review qty.