QFR No - 8000788017
Defect Details
NC No. 8000788017
NC Date 19/05/2022
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details WELDING NOT OK-WELDING BLOW HOLE AT OD SURFACE
 
1. Problem Description
Defect Description Blow Hole at OD Surface (Above the welding area)
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo pebw2vym4iu2pqxmtsmh5bjd.png
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
1000
0
2000
2000
5000
Check Qty
0
1000
0
2000
2000
5000
NG Qty
0
0
0
0
5
5
 
Scrap 5
Rework 0
Under Deviation 0
Containment Action
ALL MATERIAL SEGREGATED
 
3. Process Flow
Process Flow Description
10- RECEIVING INSPECTION 20- STORAGE 30-BLANK 40- U-BENDING 50-ROUNDING 60-WELDING 70- FLARING 80- ID SIZING 90-SIDE GRINDING 100-BROACHING 110-HEAD GRINDING & BUFFING 120- OUT SIDE MOVEMENT FOR PLATING 130-STORAGE & RQC OF PLATED MATERIAL 140-FINAL INSPECTION 150-PACKING & DISPATCH
 
4. Process Details
Process / Operation WELDING
Outsource No
Machine / Cell WELDING MACHINE
Machine / Cell No. MC NO-1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolTOOL WORN OUTTOOL OKO
MethodNOZZEL WAS NOT CLEANGASS FLOW IMPROPERX
ManUNTRAINED OPREATORSKILL MATRIXO
MachineUNDER/OVER CAPACITY MACHINE USEDFOUND CAPACITY WAS OKO
MaterialWRONG MATERIAL/GRADE USEDMATERIAL FOUND OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size VISUAL
7. Root Cause Analysis (Occurance)
Why 1 WELDING NOT DONE IN PART
Why 2 WELDING UNFILL
Why 3 PIN HOLES ON TO AREA
Why 4 GAS NOT PROPERLY FLOW
Why 5 NOZZEL CLEANING FRQUENCY WAS NOT DEFINED
Root Cause (Occurance) NOZZEL CLEANING FRQUENCY WAS NOT DEFINED
 
Root Cause Analysis (Outflow)
Why 1 DEFECTIVE PARTS COULD NOT DETECT DURING FINAL INSPECTION
Why 2 INSPECTOR WAS NOT AWAR ABOUT THE DEFECT
Why 3 PROBLEM FOUND FIRST TIME
Why 4
Why 5
Root Cause (Outflow) INSPECTOR WAS NOT AWAR ABOUT THE DEFECT
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNOZZEL CLEANING FRQUENCY TO DEFINEDNICE STEEL IND01/06/202201/06/2022Completed
OutflowLIMIT SAMPLES TO BE PROVIDED FOT OK AND NGNICE STEEL IND01/06/202201/06/2022Completed
OutflowONE POINT LESSON UPDATEDNICE STEEL IND01/06/202201/06/2022Completed
OutflowTRAINING PROVIDED TO ALL CONCERN PERSONNICE STEEL IND01/06/202201/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% VISUAL INSPECTION STARTED
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size VISUAL
10. Evidance of Countermeasure
Occurance (Before) NA
138_Occurance_Before.jpg
Occurance (After) NOZZALE CLEANING FRQUENCY DEFINED
138_Occurance_After.pdf
Outflow (Before) NA
138_Outflow_Before.jpg
Outflow (After) 1-TRAINING PROVIDED TO ALL 2- OPL DISPLAYED
138_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 6000
Reason for submission Verified qty of 6000 Nos by 100% inspection and found effective.