QFR No - 8000788018
Defect Details
NC No. 8000788018
NC Date 19/05/2022
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details WELDING NOT OK-WELDING SPATTER
 
1. Problem Description
Defect Description Welding Spatter at Outer Surface
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo pebw2vym4iu2pqxmtsmh5bjd.png
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
1000
0
2000
1000
4000
Check Qty
0
1000
0
2000
1000
4000
NG Qty
0
1
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
ALL MATERIAL TO BE RECHECKED
 
3. Process Flow
Process Flow Description
10- RECEIVING INSPECTION 20- STORAGE 30-BLANK 40- U-BENDING 50-ROUNDING 60-WELDING 70- FLARING 80- ID SIZING 90-SIDE GRINDING 100-BROACHING 110-HEAD GRINDING & BUFFING 120- OUT SIDE MOVEMENT FOR PLATING 130-STORAGE & RQC OF PLATED MATERIAL 140-FINAL INSPECTION 150-PACKING & DISPATCH
 
4. Process Details
Process / Operation WELDING
Outsource No
Machine / Cell WELDING
Machine / Cell No. 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWRONG MATERIAL USEDMTC VERIFIED AND FOUND OKO
ManUNTRAINED OPERATORSKILL MATRIX AVAILABLEO
MachineLOW/HIGHER CAPACITY MACHINE USEDMACHINE FOUND OKO
ToolTIP/NOZZELE WAS NOT CLEANNOZZEL CLEANING NOT DONEX
MethodPROCESS SHEET WAS NOT FOLLOWEDCHECK AND FOUND OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 WELDING SPATTER IN PART
Why 2 WELDING PARTICALS GENERATED DURING WELDING
Why 3 WELDING WIRE STUCK IN NOZZELE
Why 4 WELDING DUST IN NOZZELE
Why 5 NOZZELE WAS NOT CLEAN
Root Cause (Occurance) 1-WELDING DUST IN NOZZELE 2-NOZZELE WAS NOT CLEAN
 
Root Cause Analysis (Outflow)
Why 1 DEFECTIVE PART NOT DETECT DURING INSPECTION
Why 2 PROBLEM COULD NOT DETECT DURING SAMPLING INSPECTION
Why 3
Why 4
Why 5
Root Cause (Outflow) PROBLEM COULD NOT DETECT DURING SAMPLING INSPECTION
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNOZZELE CLEAING FREQUENCY TO BE DEFINEDNICE STEEL01/09/202214/06/2022Completed
OutflowOPL DISPLAYED AND 100% VISUAL INSEPCTION STARTEDNICE01/09/202214/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% VISUAL INSPECTION
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size VISUAL
10. Evidance of Countermeasure
Occurance (Before) MACHINE CHECKSHEET ATTACHED
139_Occurance_Before.pdf
Occurance (After) MACHINE CHECKSHEET ATTACHED
139_Occurance_After.pptx
Outflow (Before) NO ANY DOCUMENTS
139_Outflow_Before.pdf
Outflow (After) OPL ATTACHED
139_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant ....
 
12. Document Review
Documents PMCheckSheet, WISOP, JHCheckSheet
Specify Other Document TRAINING RECORDS
 
13. Effectiveness Of Action
Reviewed Quantity 10500
Reason for submission Reviewed quantity and found not repeated