QFR No - 8000788018
Defect Details
NC No. | 8000788018 |
NC Date | 19/05/2022 |
NC Submission Date | |
Part No. | S1AB00612B |
Part Name | ADJUSTER PLATED |
Supplier Name & Code | 100782-NICE STEEL INDUSTRIES |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | WELDING NOT OK-WELDING SPATTER |
1. Problem Description
Defect Description | Welding Spatter at Outer Surface |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | pebw2vym4iu2pqxmtsmh5bjd.png |
Supplier Communication Details
Quality Head Email ID | ppc.nice@batragroup.biz |
Plant Head/CEO Email ID | ho.nice@batragroup.biz |
MD Email ID | hitesh@batragroup.biz |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
1000
|
0
|
2000
|
1000
|
4000
|
Check Qty |
0
|
1000
|
0
|
2000
|
1000
|
4000
|
NG Qty |
0
|
1
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
ALL MATERIAL TO BE RECHECKED |
3. Process Flow
Process Flow Description |
---|
10- RECEIVING INSPECTION 20- STORAGE 30-BLANK 40- U-BENDING 50-ROUNDING 60-WELDING 70- FLARING 80- ID SIZING 90-SIDE GRINDING 100-BROACHING 110-HEAD GRINDING & BUFFING 120- OUT SIDE MOVEMENT FOR PLATING 130-STORAGE & RQC OF PLATED MATERIAL 140-FINAL INSPECTION 150-PACKING & DISPATCH |
4. Process Details
Process / Operation | WELDING |
Outsource | No |
Machine / Cell | WELDING |
Machine / Cell No. | 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | WRONG MATERIAL USED | MTC VERIFIED AND FOUND OK | O |
Man | UNTRAINED OPERATOR | SKILL MATRIX AVAILABLE | O |
Machine | LOW/HIGHER CAPACITY MACHINE USED | MACHINE FOUND OK | O |
Tool | TIP/NOZZELE WAS NOT CLEAN | NOZZEL CLEANING NOT DONE | X |
Method | PROCESS SHEET WAS NOT FOLLOWED | CHECK AND FOUND OK | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | WELDING SPATTER IN PART |
Why 2 | WELDING PARTICALS GENERATED DURING WELDING |
Why 3 | WELDING WIRE STUCK IN NOZZELE |
Why 4 | WELDING DUST IN NOZZELE |
Why 5 | NOZZELE WAS NOT CLEAN |
Root Cause (Occurance) | 1-WELDING DUST IN NOZZELE 2-NOZZELE WAS NOT CLEAN |
Root Cause Analysis (Outflow)
Why 1 | DEFECTIVE PART NOT DETECT DURING INSPECTION |
Why 2 | PROBLEM COULD NOT DETECT DURING SAMPLING INSPECTION |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | PROBLEM COULD NOT DETECT DURING SAMPLING INSPECTION |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | NOZZELE CLEAING FREQUENCY TO BE DEFINED | NICE STEEL | 01/09/2022 | 14/06/2022 | Completed |
Outflow | OPL DISPLAYED AND 100% VISUAL INSEPCTION STARTED | NICE | 01/09/2022 | 14/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% VISUAL INSPECTION |
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | VISUAL |
10. Evidance of Countermeasure
Occurance (Before) |
MACHINE CHECKSHEET ATTACHED 139_Occurance_Before.pdf |
Occurance (After) |
MACHINE CHECKSHEET ATTACHED 139_Occurance_After.pptx |
Outflow (Before) |
NO ANY DOCUMENTS 139_Outflow_Before.pdf |
Outflow (After) |
OPL ATTACHED 139_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | .... |
12. Document Review
Documents | PMCheckSheet, WISOP, JHCheckSheet |
Specify Other Document | TRAINING RECORDS |
13. Effectiveness Of Action
Reviewed Quantity | 10500 |
Reason for submission | Reviewed quantity and found not repeated |