QFR No - 8000788086
Defect Details
NC No. 8000788086
NC Date 19/05/2022
NC Submission Date
Part No. C3MD00402B
Part Name COMPRESSION SPRING 64kg
Supplier Name & Code 100185-HELICAL SPRINGS
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details MISSMATCH-WIRE DIA OBS 1.78 AGAINST 1.90+/-0.03MM
 
1. Problem Description
Defect Description Wire dia observed 1.78 against 1.90+/-0.03 mm
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Prabhat@helicalsprings.in
Plant Head/CEO Email ID awadhwa@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
18000
0
18000
Check Qty
0
0
0
5000
0
5000
NG Qty
0
0
0
2
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
Segregation of material at helical end found no part NG
 
3. Process Flow
Process Flow Description
RM->COILING->SR1->GRINDING->SHOT -PEENING->SR2->FINAL INSPECTION->SURFACE FINISHING(OILING)->DESPATCH\PACKING
 
4. Process Details
Process / Operation PACKING\DESPATCH
Outsource No
Machine / Cell NONE
Machine / Cell No. NONE
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNEW OPERATORNO NEW MANPOER.ALL MANPOWER MIN. 2 YEAR EXPERIENCEDO
MethodERROR IN INSPECTIONWIRE DIA CHECK AT COILING STATION FOUND OKO
MethodSIMILIAR PART MIXUPLEF OUT PART OF WIRE DIA 1.90 STORE IN RACK AND 1.8 WIRE DIA IS ALSO STOREO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 Wire dia 1.80 mm AGAINST 1.90MM (MIX-UP)
Why 2 Different model Spring got mixed up during packing
Why 3 Both springs are same in Geometrically
Why 4 unidentified other model (left out parts) loose springs packed during packing.
Why 5 All model Springs left out parts are store in single racks
Root Cause (Occurance) unidentified other model (left out parts) loose springs packed during packing.
 
Root Cause Analysis (Outflow)
Why 1 Wire dia 1.80 mm AGAINST 1.90MM (MIX-UP)
Why 2 Wrong model mix -up
Why 3 Could not detect during sampling inspection
Why 4
Why 5
Root Cause (Outflow) Could not detected in sampling plan
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Training given to oiling and packing person for how to handle the loose springs. 2.)Separate packing station to be defined for both the parts.(Under discussion) 3.) Diffrent Loaction is defiend to store the bothe parts (Under discussion) 4.) Display Similar parts listArunesh31/05/202230/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details no change is inspection method
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 20
10. Evidance of Countermeasure
Occurance (Before) location not defined
129_Occurance_Before.jpg
Occurance (After) location defined
129_Occurance_After.jpg
Outflow (Before) wire dia not checking at final inspection
129_Outflow_Before.jpg
Outflow (After) wire dia checking at final inspection as per sampling
129_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant similar part matrix displayed
 
12. Document Review
Documents PFMEA
Specify Other Document Work instruction
 
13. Effectiveness Of Action
Reviewed Quantity 50000
Reason for submission Inspection side action not full proof need 100% inspection for ID to catch wire dia variation