QFR No - 8000788173
Defect Details
NC No. 8000788173
NC Date 20/05/2022
NC Submission Date
Part No. 550BZ01402
Part Name CAP OIL LOCK - DF01
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-OD OVERSIZED DIMN 7MM OVERSIZE STEP ON T
 
1. Problem Description
Defect Description OD 18mm oversized by 0.15mm & Dimn 7mm Undersized/oversized
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 3158
Is Defect Repeatative? Yes
Defect Sketch / Photo jq1zd3jwbvlx5fndf34ouof2.pptx
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
0
0
5000
6000
16000
Check Qty
5000
0
0
5000
6000
16000
NG Qty
3158
0
0
0
15
3173
 
Scrap 8
Rework 3165
Under Deviation 0
Containment Action
On job training given to operator & lock and key box provided for setting pieces. OPL displayed on machine stage for awareness purpose.
 
3. Process Flow
Process Flow Description
10)- RM Inward inspection, 20)- Parting ,Drilling & angle 1.4°, 30)- Ø8.50 & Ø14.04 chamfering, 40)-Grinding Operation,50)-Plating, 60)-Final Inspection, 70)-Pre-dispatch inspection., 80)-Packing & Dispatch.
 
4. Process Details
Process / Operation Parting and drilling operation.
Outsource No
Machine / Cell Traub Machining shop
Machine / Cell No. SE/A/05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWrong material usedRaw material test certificate verified by in process quality engineers & Third part report evident.O
MethodSetting piece mix upSetting pieces got mix up with ok material, Lock and key not exist for Rework and rejection parts.X
MachineInaccurate machinePreventive maintenance monitoring on half yearly basis & record evident as per planO
Mansemi-skilled manpower, operator fluctuationOperator having inadequate knowledge of operation & Rework/Rejection part disposalX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 Depth 7.0+/-0.1 O/s
Why 2 Setting piece mix up
Why 3 Lock & Key not done for setting pieces
Why 4
Why 5
Root Cause (Occurance) Lock & Key not done for setting pieces
 
Root Cause Analysis (Outflow)
Why 1 Judgment error
Why 2 Checking By PPG
Why 3 Special dial type gauge not available.
Why 4
Why 5
Root Cause (Outflow) Special dial type gauge not available.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOn job training given to operator & lock and key box provided for setting pieces. OPL displayed on machine stage for awareness purpose.Mr. Shaikh Laik25/05/202226/05/2022Completed
OutflowDial type gauge made available & Stage wise skill matrix monitoring and Q gate license implemented for inspectors. OPL displayed for awareness .Mr. Shaikh Laik25/05/202226/05/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details M/s Sharp made available Spl. Dial type gauge for DIM 7.0+/-0.1 mm checking at final & in process inspection stage to avoid man oriented inspection. Gauge implemented & checking on daily basis.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 100:1200
10. Evidance of Countermeasure
Occurance (Before) Lock & Key not done for setting pieces, Open red and yellow bin provided for setting/NG pieces.
130_Occurance_Before.pptx
Occurance (After) Rejection & Rework material kept in lock & key on machine to avoid mix up issue.
130_Occurance_After.pptx
Outflow (Before) 1. Relation gauge used for checking 100% parts but not effective by vernier caliper, Detection side inspection being done by attribute type gauge.
130_Outflow_Before.pptx
Outflow (After) M/s Sharp made available Spl. Dial type gauge for DIM 7.0+/-0.1 mm checking at final & in process inspection stage to avoid man oriented inspection. Gauge implemented & checking on daily basis.
130_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CAP OIL LOCK LML/DF & PRF
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document NIL
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission Ok