QFR No - 8000789394
Defect Details
NC No. | 8000789394 |
NC Date | 30/05/2022 |
NC Submission Date | |
Part No. | S2BY03451B |
Part Name | CANISTER SQR GROOVE LEAK TESTED |
Supplier Name & Code | 100465-PN DIE CASTINGS PVT LTD |
ETL Plant | 1126-ETL Pantnagar |
Defect Details | DIMN.O/SIZE.-GR0OVE WIDTH OVERSIZE |
1. Problem Description
Defect Description | Groove Dim. 4.10+0.10 observed upto 4.32,4.40,4.45 and the Step height 2±0.10 just below the Groove observed as 1.64,1.53,1.62. and Dim. 1.50+0.10 observed as 1.24,1.36,1.31 |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1335 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qualityqh@bansaldiecastings.com |
Plant Head/CEO Email ID | gm@bansaldiecastings.com |
MD Email ID | piyush@bansaldiecastings.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
0
|
0
|
3000
|
100
|
4600
|
Check Qty |
1500
|
0
|
0
|
3000
|
100
|
4600
|
NG Qty |
1500
|
0
|
0
|
3000
|
100
|
4600
|
Scrap | 4600 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
1.Segrigated all store ,wip & Assly area at customer end(1500 qty) by the leak testing machine and found All part not ok- Akshay 2.Segrigated all store & wip at BDC end(3100 qty) by the HG & VC 60 nos and 3040 nos by template ,found All part not ok- Bhuvan |
3. Process Flow
Process Flow Description |
---|
10.RM receiving & inspection 20.Die casting & inspection 30.Fettling & Filing 40.Shot blasting 50.Drilling 60.VMC machining......(Incident station) 70.Air cleaning 80.Impregnation 90.Pin Pressing 100.Leak Testing 110.Final inspection 120.Packing & storage 130.Dispatch |
4. Process Details
Process / Operation | Machining/Grooving |
Outsource | No |
Machine / Cell | VMC09/Machining |
Machine / Cell No. | VMC09/B03 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Groove tool not ok | Groove tool inspection not done | X |
Machine | Vibration in machine, new machine, New Fixture | PM check sheet & 4M verified , Found ok | O |
Material | Wrong grade | MTC & LTC verified , Found ok | O |
Man | Untrained operator/ inspector | Skill matrix verified & found ok | O |
Method | Groove inspection is not done during FPA | FPA report verified & found groove inspection point missing | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | First peace approval |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 0 |
7. Root Cause Analysis (Occurance)
Why 1 | Leakage in Canister |
Why 2 | Groove O Ring loose |
Why 3 | Groove width over size |
Why 4 | Groove tool not ok |
Why 5 | |
Root Cause (Occurance) | Groove tool not Ok |
Root Cause Analysis (Outflow)
Why 1 | Leakage in Canister |
Why 2 | Groove O Ring loose |
Why 3 | Groove width over size |
Why 4 | Groove width inspection Point miss in FPA report & PDI report |
Why 5 | |
Root Cause (Outflow) | Groove width inspection Point miss in FPA report |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1.Quality alert 2. Tool incoming inspection report 3.Set up approval report | Abhay saxena & Akshay | 02/06/2022 | 02/06/2022 | Completed |
Outflow | 1.OPL 2.OJT 3.Point Add in FPA Report 4.Point add in PDI report | Akshay | 03/06/2022 | 03/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1.1 no`s groove width inspection in every shift(During FPA) by VC in every shift after parting of sample part . 2. 1 no`s groove width inspection in every lot(During PDI) by VC in every lot after parting of sample part . |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 1 |
10. Evidance of Countermeasure
Occurance (Before) |
No tool Inspection report 156_Occurance_Before.xlsx |
Occurance (After) |
Tool inspection report available 156_Occurance_After.xlsx |
Outflow (Before) |
Groove width inspection Point miss in FPA report & PDI report 156_Outflow_Before.xlsx |
Outflow (After) |
Groove width inspection Point miss added in FPA report & PDI report 156_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | No |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, AuditCheckSheet, InspCheckSheet |
Specify Other Document | FPA & PDI report |
13. Effectiveness Of Action
Reviewed Quantity | 1 |
Reason for submission | Found OK |