QFR No - 8000789590
Defect Details
NC No. 8000789590
NC Date 31/05/2022
NC Submission Date
Part No. 550LG06202
Part Name SEAT PIPE -K23A/PRFH-006
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1116-ETL K-120 Suspension
Defect Details RUN OUT MORE-RUNOUT OVERSIZE. 0.5 AGAINST 0.1 MAX
 
1. Problem Description
Defect Description M8 threading runout wrt to outer dia. observed up to 0.55, 0.5 mm against drg. requirement of 0.1 mm. This concern leads to assembly movement NG as well as noise concern.
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1700
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1700
1500
0
0
0
3200
Check Qty
15
0
0
0
0
15
NG Qty
15
0
0
0
0
15
 
Scrap 0
Rework 0
Under Deviation 15
Containment Action
Segregated all parts at ETL, at Warehouse & at NPC Nabha.
 
3. Process Flow
Process Flow Description
1.Raw Material 2.Cutting & Chemfering 3.Multistation Draw 4.Head Formation 5.Rough Grinding 6.Punching 7.CNC Head Turning 8.CNC Boring & Facing 9.Tapping 10.Chemfering 1&2 11.Finish Grinding 12.Final Inspection 13.Cleaning 14.Oiling 15.Packing &Dispatch
 
4. Process Details
Process / Operation CNC Boring & Facing
Outsource No
Machine / Cell CNC
Machine / Cell No. NPC/CNC/011
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Methodskipped at final inspectionit was observed that parts skipped during sampling at final inspection.X
ManIn process operator negligentoperator was aware about the defect he found to be non negligentO
MachineGrinding wheel center outGrinding wheel was not center outO
Materialcollet sleeve damageCollet sleeve wearoutX
Machinegrinding wheel will good condition.grinding wheel was not dressO
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size ssp (0.65)
7. Root Cause Analysis (Occurance)
Why 1 collet sleeve was damage.
Why 2 Collet sleeve wearout during CNC boring operation
Why 3 collet sleeve was not change.
Why 4 collet sleeve was wear out before expiry
Why 5
Root Cause (Occurance) collet was wear out before expiry
 
Root Cause Analysis (Outflow)
Why 1 run out oversize.
Why 2 Could not be detected at final inspection.
Why 3 skipped at final inspection.
Why 4 Skipped in Sampling inspection.
Why 5
Root Cause (Outflow) Skipped in Sampling inspection.k
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowSampling plan doubled.Mr. Gurpreet21/06/202220/06/2022Completed
OccuranceReduce life cycle time of collet sleeve after validation.Gursewak singh24/06/202222/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details sampling plan double.
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size double
10. Evidance of Countermeasure
Occurance (Before) collet sleeve was wear out before expiry
159_Occurance_Before.jpg
Occurance (After) Collet sleeve is change after life time reduce (according to new validation)
159_Occurance_After.jpg
Outflow (Before) Skipped in Sampling inspection.
159_Outflow_Before.jpg
Outflow (After) Sampling inspection doubled
159_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CNC Machine
 
12. Document Review
Documents ControlPlan, PMCheckSheet, WISOP, JHCheckSheet, ProcessFlowChart, InspCheckSheet
Specify Other Document validation report
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission No any improvement observed in received lots.