QFR No - 8000789810
Defect Details
NC No. | 8000789810 |
NC Date | 02/06/2022 |
NC Submission Date | |
Part No. | B2GQ03323O |
Part Name | M/CYL BODY RAW POW.COATED-RE J1C FRONT |
Supplier Name & Code | 100204-KRISHNA COATING |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | POWDER COATING NOT OK-AFTER100%INSP.DUST,UNCOVER,BUBBLE |
1. Problem Description
Defect Description | Dust and uncover |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 60 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qualitykrishnaassociates01@gmail.com |
Plant Head/CEO Email ID | ravikrishnacoating@gmail.com |
MD Email ID | krishnacoating@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4448
|
0
|
0
|
0
|
0
|
4448
|
Check Qty |
4448
|
0
|
0
|
0
|
0
|
4448
|
NG Qty |
125
|
0
|
0
|
0
|
0
|
125
|
Scrap | 0 |
Rework | 125 |
Under Deviation | 0 |
Containment Action |
---|
before sampling basis Inspection done at inward stage. but currently we start 100 % raw material Inspection at inward inspection stage |
3. Process Flow
Process Flow Description |
---|
Inward -100 % visual inspection - Pretreatment - Drying - Powder coating - Baking - final inspection - packing & dispatch |
4. Process Details
Process / Operation | Powder Coating |
Outsource | No |
Machine / Cell | Powder coating line |
Machine / Cell No. | Powder coating line |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Rusty material , oily , | Rusty material observed at inward stage | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
7. Root Cause Analysis (Occurance)
Why 1 | Bubble defect observed |
Why 2 | White rust observe in master cylinder RE- J1C at inward stage |
Why 3 | no 100 % visual inspection plan at inward stage |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | White rusty part observe at inward inspection stage |
Root Cause Analysis (Outflow)
Why 1 | rusty material observed |
Why 2 | Only inward inspection on sampling basis |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Rusty Material |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Now we started 100% visual inspection at inward stage | Ahok dabhade | 04/07/2022 | 05/07/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% visual Inspection at inward stage |
Inspection Method | Other |
Other Inspection Method | VIsual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
only sampling basis inward inspection at inward stage 161_Occurance_Before.pdf |
Occurance (After) |
Now Started 100 % visual inspection at inward stage ( as per sampling plan ) 161_Occurance_After.pdf |
Outflow (Before) |
only sampling basis inward inspection at inward stage 161_Outflow_Before.pdf |
Outflow (After) |
Now Started 100 % visual inspection at inward stage ( as per sampling plan 161_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | inward stage |
12. Document Review
Documents | WISOP |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 1360 |
Reason for submission | No rusty found in next 3 lot |