QFR No - 8000790294
Defect Details
NC No. 8000790294
NC Date 07/06/2022
NC Submission Date
Part No. S1JL02405B
Part Name PISTON ROD PLATED K0LA
Supplier Name & Code 100953-PACE AUTOPARTS PRIVATE LIMITED
ETL Plant 1136-ETL Suspension Sanand
Defect Details LENGTH OVERSIZE-TOTAL LENGTH OVERSIZE
 
1. Problem Description
Defect Description Length Over Size
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 140
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qa@paceautoparts.in
Plant Head/CEO Email ID sudhakar.chavan@paceautoparts.in
MD Email ID jadhav@paceautoparts.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4200
0
10000
2520
0
16720
Check Qty
4200
0
10000
2520
0
16720
NG Qty
140
0
0
0
0
140
 
Scrap 0
Rework 0
Under Deviation 140
Containment Action
All quantity available at end checked for reported concern issue & no any found defective quantity.
 
3. Process Flow
Process Flow Description
Cutting- CNC machining-I - Rough grinding-I -Rough grinding-II - CNC machining -II - Thread rolling- I- thread rolling-II - Semi finish grinding-Finish grinding - Hard chrome plating- Superfinishing process- Final inspection - packing- Dispatch
 
4. Process Details
Process / Operation Packing
Outsource No
Machine / Cell Packing
Machine / Cell No. packing-I
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper material handlingImproper material handlingO
MethodMultiple items handled same time at packagingMultiple items handled same time at packagingO
MethodSimilar location for itemsSimilar location for itemsO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method 100 % box weight
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 Multiple items handled same time at packaging
Why 2 Similar locations for items
Why 3 care not to be taken during packaging
Why 4 Lack of awareness
Why 5
Root Cause (Occurance) operator negligence
 
Root Cause Analysis (Outflow)
Why 1 Lack of awareness
Why 2 Negligence
Why 3
Why 4
Why 5
Root Cause (Outflow) Negligence
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWe had started the box weight 200 %& displayed the weight chart at weighing machineStore10/06/202207/06/2022Completed
OccuranceWe had implemented the one item packaging at a single time & on only line single model will be placed for final inspection also.Final inspection15/06/202210/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No any change in inspection system.
Inspection Method Other
Other Inspection Method 200 % box weight
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Box weight done 100 % at the time of dispatch & multiple items for packaging at a time
163_Occurance_Before.jpg
Occurance (After) We have started the box weight 200 % at the time of dispatch & box weight chart displayed at weighing machine & On final inspection table single component will be checked & packed.
163_Occurance_After.jpg
Outflow (Before) Improper material handling
163_Outflow_Before.jpg
Outflow (After) Training given to operator regarding concern issue & proper material handling ..
163_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Horizontally deployed for all parts
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document DOC AUDIT
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Closed