QFR No - 8000790951
Defect Details
NC No. 8000790951
NC Date 11/06/2022
NC Submission Date
Part No. F2LY02502B
Part Name SOCKET HEADED BOLT - RE J1A
Supplier Name & Code 100846-SANGKAJ ENGINEERING PVT.LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-PLATING THICKNESS LESS
 
1. Problem Description
Defect Description Zinc Plating Thickness Less
Detection Stage Customer End
Problem Severity Function
NG Quantity 23200
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID vishwas@sangkaj.com
Plant Head/CEO Email ID pardeshinr@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
24800
0
0
400
3700
28900
Check Qty
50
0
0
5
10
65
NG Qty
10
0
0
0
0
10
 
Scrap 10
Rework 0
Under Deviation 0
Containment Action
All finish stage material taken for plating rework from ETL and SEPL, as it is not possible to verify 100% for plating thickness
 
3. Process Flow
Process Flow Description
Raw material inward--wire draw--Forging--Rolling--Heat treatment--plating- final inspection and PDI--packing and dispatch
 
4. Process Details
Process / Operation Plating process
Outsource Yes
Machine / Cell Outsource
Machine / Cell No. Outsource
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Methodprocess parameters are not as per specificationvalidation check for corrected parametersX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method XRF inspection
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10nos
7. Root Cause Analysis (Occurance)
Why 1 Low thickness observed on plated components
Why 2 Process done on parts as per regular lot size
Why 3 Because of small parts its required different lot size & current supply
Why 4 Proper validation not done for small parts
Why 5 during validation thickness checked on regular DFT which shows OK reading
Root Cause (Occurance) 1) Proper validation not done for small parts. 2) Parts checked on regular thickness tester.
 
Root Cause Analysis (Outflow)
Why 1 Low thickness observed on plated components
Why 2 Not detected by regular thickness tester ( DFT)
Why 3 XRF thickness reading is less than regular thickness tester reading
Why 4
Why 5
Root Cause (Outflow) XRF thickness reading is less than regular thickness tester reading
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePlating will done on Valid parameters & its records maintained as per requirements .M/S Krishna Indstires13/06/202212/06/2022Completed
Outflowchecking done on XRF thickness tester before dispatch the material ,M/S Krishna Industires13/06/202212/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Plating thickness checking start with XRF on sampling basis
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10nos
10. Evidance of Countermeasure
Occurance (Before) Validation not done properly
172_Occurance_Before.pptx
Occurance (After) Proper validation done for small parts
172_Occurance_After.pdf
Outflow (Before) Checking method by regular DFT meter
172_Outflow_Before.pdf
Outflow (After) Checking method change to XRF from regular DFT meter
172_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All small parts
 
12. Document Review
Documents ControlPlan, WISOP, InspCheckSheet
Specify Other Document Validation document
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission Ok