QFR No - 8000790951
Defect Details
NC No. | 8000790951 |
NC Date | 11/06/2022 |
NC Submission Date | |
Part No. | F2LY02502B |
Part Name | SOCKET HEADED BOLT - RE J1A |
Supplier Name & Code | 100846-SANGKAJ ENGINEERING PVT.LTD. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-PLATING THICKNESS LESS |
1. Problem Description
Defect Description | Zinc Plating Thickness Less |
Detection Stage | Customer End |
Problem Severity | Function |
NG Quantity | 23200 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | vishwas@sangkaj.com |
Plant Head/CEO Email ID | pardeshinr@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
24800
|
0
|
0
|
400
|
3700
|
28900
|
Check Qty |
50
|
0
|
0
|
5
|
10
|
65
|
NG Qty |
10
|
0
|
0
|
0
|
0
|
10
|
Scrap | 10 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All finish stage material taken for plating rework from ETL and SEPL, as it is not possible to verify 100% for plating thickness |
3. Process Flow
Process Flow Description |
---|
Raw material inward--wire draw--Forging--Rolling--Heat treatment--plating- final inspection and PDI--packing and dispatch |
4. Process Details
Process / Operation | Plating process |
Outsource | Yes |
Machine / Cell | Outsource |
Machine / Cell No. | Outsource |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | process parameters are not as per specification | validation check for corrected parameters | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | XRF inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10nos |
7. Root Cause Analysis (Occurance)
Why 1 | Low thickness observed on plated components |
Why 2 | Process done on parts as per regular lot size |
Why 3 | Because of small parts its required different lot size & current supply |
Why 4 | Proper validation not done for small parts |
Why 5 | during validation thickness checked on regular DFT which shows OK reading |
Root Cause (Occurance) | 1) Proper validation not done for small parts. 2) Parts checked on regular thickness tester. |
Root Cause Analysis (Outflow)
Why 1 | Low thickness observed on plated components |
Why 2 | Not detected by regular thickness tester ( DFT) |
Why 3 | XRF thickness reading is less than regular thickness tester reading |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | XRF thickness reading is less than regular thickness tester reading |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Plating will done on Valid parameters & its records maintained as per requirements . | M/S Krishna Indstires | 13/06/2022 | 12/06/2022 | Completed |
Outflow | checking done on XRF thickness tester before dispatch the material , | M/S Krishna Industires | 13/06/2022 | 12/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Plating thickness checking start with XRF on sampling basis |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10nos |
10. Evidance of Countermeasure
Occurance (Before) |
Validation not done properly 172_Occurance_Before.pptx |
Occurance (After) |
Proper validation done for small parts 172_Occurance_After.pdf |
Outflow (Before) |
Checking method by regular DFT meter 172_Outflow_Before.pdf |
Outflow (After) |
Checking method change to XRF from regular DFT meter 172_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All small parts |
12. Document Review
Documents | ControlPlan, WISOP, InspCheckSheet |
Specify Other Document | Validation document |
13. Effectiveness Of Action
Reviewed Quantity | 150 |
Reason for submission | Ok |