QFR No - 8000791480
Defect Details
NC No. 8000791480
NC Date 15/06/2022
NC Submission Date
Part No. S1AB00307B
Part Name ADJUSTER POWDER COATED K0LA
Supplier Name & Code 100973-ABHIVRDHI ENGINEERING PRIVATE
ETL Plant 1136-ETL Suspension Sanand
Defect Details POWDER COATING NOT OK-POWDERCOATING PROBLEM
 
1. Problem Description
Defect Description Powder Coating defects like paint bubble, paint dry, paint dust etc. and wrong supplier code (found V code instead of A code)
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 275
Is Defect Repeatative? No
Defect Sketch / Photo 0s4yuyooyw4vtdtqjaz2mq3a.jpg
Supplier Communication Details
Quality Head Email ID rkhare@tesmomotorcast.com
Plant Head/CEO Email ID harish.bala@tesmomotorcast.com
MD Email ID svkallani@tesmomotorcast.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
275
0
0
0
2100
2375
Check Qty
275
0
0
0
2100
2375
NG Qty
275
0
0
0
0
275
 
Scrap 75
Rework 150
Under Deviation 50
Containment Action
After powder coated 100% inspection
 
3. Process Flow
Process Flow Description
pdc - ,reming - od grinding, - debering - surface treatment - inspection - powder coated - packing.
 
4. Process Details
Process / Operation Powder Coated
Outsource Yes
Machine / Cell booth 1
Machine / Cell No. 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Methodnot proper spraygaugeO
MethodPre-Treatment process not donesystemO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1
7. Root Cause Analysis (Occurance)
Why 1 Powder coating not ok
Why 2 Powder not uniform on part
Why 3 Powder electrostatic gun malfunctioning
Why 4 Gun to earth continuity not good
Why 5 Continuity pm not check
Root Cause (Occurance) point not available in pm check sheet
 
Root Cause Analysis (Outflow)
Why 1 powder coating not ok
Why 2 Uncover part in final packing
Why 3 100 % inspection not happen after powder coating
Why 4 Sample inspection process follow
Why 5 Inspection system not ok
Root Cause (Outflow) 100% inspection started
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceContinuity checking from gun to hanger startedRahul06/03/2023Completed
Outflow100 % inspection startedRahul06/03/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection after powder coating
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1
10. Evidance of Countermeasure
Occurance (Before) Before powder coated
180_Occurance_Before.jpg
Occurance (After) after powder coated
180_Occurance_After.jpg
Outflow (Before) powder coated check
180_Outflow_Before.jpg
Outflow (After) 100% inspection check
180_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant adjuster kola
 
12. Document Review
Documents ControlPlan, PackingStd
Specify Other Document process flow chart
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission