QFR No - 8000793197
Defect Details
NC No. 8000793197
NC Date 27/06/2022
NC Submission Date
Part No. S1GD01726B
Part Name INNER TUBE CHAMFERED K0LA
Supplier Name & Code 100165-SAPTAGIRI INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details HIGHT O/SIZE.-TOTAL LENGTH LESS&MORE
 
1. Problem Description
Defect Description inner tube total length less issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 121
Is Defect Repeatative? Yes
Defect Sketch / Photo 1aq54fznl1qpruyaavnfmmtb.xlsx
Supplier Communication Details
Quality Head Email ID quality@saptagirigroup.in
Plant Head/CEO Email ID production@saptagirigroup.in
MD Email ID argandhi@saptagirigroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
2000
0
0
2000
7000
Check Qty
3000
2000
0
0
2000
7000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
100 % verify all material at all location and observed 02 nos NG
 
3. Process Flow
Process Flow Description
RM receipt & Inspection , Cutting , Chamfer at both end , Straightness inspection , Packing
 
4. Process Details
Process / Operation Tube Cutting
Outsource No
Machine / Cell Troub machine
Machine / Cell No. Troub machine 04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodTotal length checking special gauge ware outGauge verified by height gauge and its observed okO
MachineSet up part mix up with OK materialRed bin with lock and key it’s missing at the machineO
MachineStopper locking loosed while tube cuttingNot loosed the stopper while tube cuttingO
MachineEnd piece mix up with OK materialFor storing end pieces one gunny bag available with identifiedO
MethodLength checking not done adequatelyLength checking done adequalityO
ManInspector not aware about total lengthOperator and inspector nor a aware about the total length special gauge and its operatingO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Total length U/s
Why 2 Set up part mix up with OK material
Why 3 Set up part storing bin missing
Why 4 No Lock & Key for storing set up or rejected parts
Why 5
Root Cause (Occurance) No Lock & Key for storing set up or rejected parts
 
Root Cause Analysis (Outflow)
Why 1 Total length U/s
Why 2 Operator not aware about total length
Why 3
Why 4
Why 5
Root Cause (Outflow) Operator not aware about total length
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance) Provide Lock & key Rejection storage binMr. Munja Hore29/06/202230/06/2022Completed
Occurance) Provide the stopper slot on chamfer machineMr. Munja Hore29/06/202230/06/2022Completed
Occurance) Make SOP for Tube Cutting operation & its verificationMr. Munja Hore29/06/202230/06/2022Completed
OutflowVerify Gauge Length. Started 100% inspection for length verification.Mr. Munja Hore29/08/202230/06/2022Completed
OutflowAwareness Training given to concern operator & InspectorMr. Munja hore29/08/202230/06/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % inspection started by special total length gauge
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Set part storage bin missing ( Not available at machine ) , no lock & key equipment for keeping rejection or set up piece
190_Occurance_Before.pdf
Occurance (After) Provided lock & key equipment for keeping rejection or set up piece
190_Occurance_After.pdf
Outflow (Before) Inspector not aware about total length and checking method
190_Outflow_Before.pdf
Outflow (After) Awareness training given to concern inspector & OPL display at work place , Made SOP for length checking gauge and same awareness given
190_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Other machine operator and inspector
 
12. Document Review
Documents ControlPlan
Specify Other Document Control plan
 
13. Effectiveness Of Action
Reviewed Quantity 12600
Reason for submission Effectiveness monitored 4 lots and no defect repeated