QFR No - 8000795498
Defect Details
NC No. | 8000795498 |
NC Date | 18/07/2022 |
NC Submission Date | |
Part No. | 550LG06202 |
Part Name | SEAT PIPE -K23A/PRFH-006 |
Supplier Name & Code | 100929-HARSHAD ENGINEERING COMPANY |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | MIX UP OTHER MODEL-LENGTH LESS MIX UP NOT USING KON MODEL |
1. Problem Description
Defect Description | KON front fork seat pipe total length less mix up repeated issue compression one through hole available |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 50 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | hy34ct1limjq3bxzxoomdguv.xlsx |
Supplier Communication Details
Quality Head Email ID | qaharshad@gmail.com |
Plant Head/CEO Email ID | qaharshad@gmail.com |
MD Email ID | auto.mitesh@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4000
|
0
|
0
|
2150
|
5550
|
11700
|
Check Qty |
4000
|
0
|
0
|
0
|
0
|
4000
|
NG Qty |
20
|
0
|
0
|
0
|
0
|
20
|
Scrap | 20 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % sorting done for ETL End, HEC WIP & FG material |
3. Process Flow
Process Flow Description |
---|
Cutting-Draw-Forging(Head Formation)-Rough Grinding-CNC (Head, Boring & Tapping)-Punching-Finish Grinding-Final Inspection-Packing-Dispatch |
4. Process Details
Process / Operation | Inspection & packing |
Outsource | No |
Machine / Cell | Packing & Inspection |
Machine / Cell No. | 120-A & B |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Mix-up while packing & Inspection | Mix-up while polybag filling& Packing | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
7. Root Cause Analysis (Occurance)
Why 1 | Mix-up with other model |
Why 2 | Mix-up while packing |
Why 3 | No separate color identification to polybag |
Why 4 | use standard polybag for packing |
Why 5 | |
Root Cause (Occurance) | No separate color identification to polybag |
Root Cause Analysis (Outflow)
Why 1 | Mix-up with other model |
Why 2 | While polybag sealing manual parts counting done |
Why 3 | weight polybag & Box not done/Measured |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | weight polybag & Box not done/Measured |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Yellow color polybag used for PRFH | VAibhav | 29/07/2022 | 27/07/2022 | Completed |
Outflow | Polybag & box weight done | Vaibhav | 29/07/2022 | 27/07/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Box wt. done after packing on weighing scale & modelwise wt. chart displayed |
Inspection Method | Other |
Other Inspection Method | Manual Polybag fill |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
standard color polybag used for all seat pipes 202_Occurance_Before.jpg |
Occurance (After) |
Yellow color polybag used for PRFH seat pipe 202_Occurance_After.jpg |
Outflow (Before) |
Box & polybag wt. not done 202_Outflow_Before.jpg |
Outflow (After) |
Box & polybag wt. done as per modelwise wt. chart 202_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Packing & Dispatch section |
12. Document Review
Documents | WISOP, ProcessFlowChart, PackingStd |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 3000 |
Reason for submission | reviewed 3000 number found ok |