QFR No - 8000795960
Defect Details
NC No. 8000795960
NC Date 18/07/2022
NC Submission Date
Part No. F2KH02002B
Part Name REBOUND SPRING -K74A
Supplier Name & Code 101159-TECHNOMAT SPRINGS
ETL Plant 1116-ETL K-120 Suspension
Defect Details DIAMETER OVER SIZE-OUTER DIA. OVERSIZE.
 
1. Problem Description
Defect Description In K74 Rebound spring (F2KH02002B) observed wtih outer dia. oversize concern. OD oversize by 0.2 to 0.3 mm.
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 10053
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@technomatsprings.com
Plant Head/CEO Email ID technomatsprings@gmail.com
MD Email ID patilsadanand@technomatsprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
15000
0
0
0
1200
16200
Check Qty
15000
0
0
0
1200
16200
NG Qty
10053
0
0
0
0
10053
 
Scrap 10053
Rework 0
Under Deviation 0
Containment Action
Check all material in house & customer end
 
3. Process Flow
Process Flow Description
RM>Coiling>B1>Grinding>shotpeening>B2>setting>visual inspection>oiling>Packing>Dispatch
 
4. Process Details
Process / Operation Coiling
Outsource No
Machine / Cell CNC Coiling
Machine / Cell No. Na
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operatorSkill evaluation done (Training to be providedX
MaterialAs per DrawingRMTC checked found okO
ToolImproper Tool UseCheck found okO
MachineCoiling MachineFound OkO
MethodImproper Material handlingMaterial handling done as per process verified found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1000
7. Root Cause Analysis (Occurance)
Why 1 OD Over Size
Why 2 Found OD over size 0.20 - 0.30 mm
Why 3 Finger tool loose.
Why 4
Why 5
Root Cause (Occurance) Finger tool loose
 
Root Cause Analysis (Outflow)
Why 1 OD Over size
Why 2 OD checking not done
Why 3
Why 4
Why 5
Root Cause (Outflow) OD Checking not done
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowOD Checking Start and training provide to visual inspection & Final inspection operatorMrs.Renuka10/08/202202/08/2022Completed
OccuranceTraining Provide to CNC operator.Mr.Santosh02/08/202203/08/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details OD Checking Start
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1000/20
10. Evidance of Countermeasure
Occurance (Before) OD Checking Frequency four hourly.
204_Occurance_Before.jpg
Occurance (After) OD Checking frequency change hourly basis & training provide to operator.
204_Occurance_After.jpg
Outflow (Before) OD checking not done at final inspection.
204_Outflow_Before.pdf
Outflow (After) OD checking start before dispatch.
204_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Rebound Spring
 
12. Document Review
Documents InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1500
Reason for submission Sustenance required.