QFR No - 8000797659
Defect Details
NC No. | 8000797659 |
NC Date | 29/07/2022 |
NC Submission Date | |
Part No. | 520BZ00102 |
Part Name | CAP OIL LOCK-LML |
Supplier Name & Code | 100503-DIVYA INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-STEP MARK & ID UNDERSIZE |
1. Problem Description
Defect Description | STEP IN BACK FACE & ID 14MM UNDERSIZED BY 0.5MM |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 351 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | production@mahavirind.co.in |
MD Email ID | rajesh@mahavirind.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2106
|
0
|
0
|
702
|
0
|
2808
|
Check Qty |
2106
|
0
|
0
|
702
|
0
|
2808
|
NG Qty |
351
|
0
|
0
|
13
|
0
|
364
|
Scrap | 62 |
Rework | 302 |
Under Deviation | 0 |
Containment Action |
---|
All Material Segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
1)RM Inward- 2)store - 3)Traub facing/Main Bore Drilling 14.02/14.14/8.5Drill F8.5/ID Chamfer/OD Chamfer - 4)Bottom Chamfer.5)OD Grinding.6) Plating .7) Final Inspection .8) Dispatch |
4. Process Details
Process / Operation | 3)Traub facing/Main Bore Drilling 14.02/14.14/8.5D |
Outsource | Yes |
Machine / Cell | Traub Section |
Machine / Cell No. | Traub No.2( A-25) |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | ID boring on traub Machine | During ID boring 14.02 Drill edges Line Marks Observed | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | .. |
7. Root Cause Analysis (Occurance)
Why 1 | Line Marks at the ID of 14.02 Main Bore |
Why 2 | Main ID boring operation on Traub machine |
Why 3 | 14.02 drill edges heavy Burr Sticked |
Why 4 | Drill Edges Fraction In at Part ID |
Why 5 | |
Root Cause (Occurance) | Main Boring ID operation Process by wrong Method Machining |
Root Cause Analysis (Outflow)
Why 1 | Line Marks at the ID of 14.02 Main Bore |
Why 2 | Not Defect In Final Inspection |
Why 3 | Final Inspector Not aware about lD Line Marks |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Final Inspector Not aware about lD Line Marks |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | ID Boring Process change Traub Machining To CNC Machining | Mr. Suresh Kapgate | 12/08/2022 | 12/08/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Visual Inspection Instead Of 20Nos Samples |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | .... |
10. Evidance of Countermeasure
Occurance (Before) |
Main boring Operation On Traub Machine 214_Occurance_Before.xlsx |
Occurance (After) |
Main Boring Operation Start on CNC machine 214_Occurance_After.xlsx |
Outflow (Before) |
Sampling Basis Visual Inspection 20nos Per Bin 214_Outflow_Before.docx |
Outflow (After) |
Main Bore ID 100% Visual inspection at Final Inspection stage. 214_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Cap Oil Locks |
12. Document Review
Documents | ControlPlan, PFMEA, ProcessFlowChart |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |