QFR No - 8000797760
Defect Details
NC No. 8000797760
NC Date 29/07/2022
NC Submission Date
Part No. 550HL00602
Part Name OIL LOCK COLLAR
Supplier Name & Code 100503-DIVYA INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-LENGTH U/S, OD O/S, EXTRA HOLE
 
1. Problem Description
Defect Description TOTAL LENGTH UNDERSIZED, O/D OVERSIZED & EXTRA HOLE PUNCHING
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID production@mahavirind.co.in
MD Email ID rajesh@mahavirind.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
600
0
0
0
0
600
Check Qty
600
0
0
0
0
600
NG Qty
4
0
0
0
0
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
All Suspected material Segregation at customer End
 
3. Process Flow
Process Flow Description
RM Inward- Store- Traub Parting - Semi finish Inward CNC-1st- CNC-2nd- Cross Hole Both sides- Deburring - OD Grinding - Plating -Final Inspection- Packing - Transport-
 
4. Process Details
Process / Operation Cross Hole Both sides
Outsource Yes
Machine / Cell Cross Hole Drilling Machine
Machine / Cell No. Drill M/C No.1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManDuring Cross hole Setting Piece MixDuring Cross Hole Drill CD distance Setiing 2pieces By mistake mix with ok material .X
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
7. Root Cause Analysis (Occurance)
Why 1 Double Cross hole
Why 2 Setting defective pcs mix with OK Material
Why 3 During the Change over CD Adjustment setting pcs mix
Why 4 Cross drill operator Semiskilled
Why 5
Root Cause (Occurance) Setting defective pcs mix with OK Material
 
Root Cause Analysis (Outflow)
Why 1 Double Cross hole
Why 2 Visual Inspection Not checking carefully
Why 3 Depend On Cross Drill Operator
Why 4 Without Identified Material Dispatch To Customer
Why 5
Root Cause (Outflow) Without Identified Material Dispatch To Customer
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1)Location Decided for Cross Hole Setting Piece and Defective Material. 2) Training To Operator. 3)Both Hole Identification Start By block markerMr.Suresh Kapgate/Mr.Pralhad Bhawar12/08/202212/08/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details After 360° Visual Inspection Identification Start to both cross hole to final Inspection Stage.
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) By Mistekly Setting Piece Mix With ok cross Hole Process Material.
215_Occurance_Before.jpg
Occurance (After) 1) Quality Alert Display .2)Training To Operator .3)Lock & key Red Box Provide on Cross hole Drill Machine. Not Need More Change In Fixture.
215_Occurance_After.jpg
Outflow (Before) Without Identification Dispatch To Customer
215_Outflow_Before.jpeg
Outflow (After) 1)100% Identification to both holes at the Final inspection Stage.2)Defected Sample Display On final Inspection Table. 3)Training To Inspector.
215_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All OLC Cross Hole Identification at the final Inspection stage Before Dispatch to the Customer
 
12. Document Review
Documents ControlPlan
Specify Other Document No Need
 
13. Effectiveness Of Action
Reviewed Quantity 300
Reason for submission Verified next 3 lot and found ok