QFR No - 8000802161
Defect Details
NC No. | 8000802161 |
NC Date | 29/08/2022 |
NC Submission Date | |
Part No. | 520FN04002 |
Part Name | HOLDER CLUTCH |
Supplier Name & Code | 100150-DHANANJAY ENTERPRISES |
ETL Plant | 1135-ETL 7/10 P Nagar |
Defect Details | DIMN.O/SIZE.-ID OVERSIZE |
1. Problem Description
Defect Description | ID OVERSIZE/UNDER SIZE ISSUE. |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 3 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qade@dhananjaygroup.com |
Plant Head/CEO Email ID | gunjalvs@dhananjaygroup.com |
MD Email ID | kandakuretn@dhananjaygroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
0
|
0
|
0
|
0
|
2000
|
Check Qty |
2000
|
0
|
0
|
0
|
0
|
2000
|
NG Qty |
3
|
0
|
0
|
0
|
0
|
3
|
Scrap | 3 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregate the whole lot at the ETL End/DEPL End |
3. Process Flow
Process Flow Description |
---|
Blanking/Piercing_Deburring_Chamfering_CNC Machining_Final Inspection_Cleaning_Dispatch |
4. Process Details
Process / Operation | CNC Machining |
Outsource | No |
Machine / Cell | CNC Machining |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | in final inspection Air Plug gauge Skipped by the inspector | as final inspection (Air Plug Gauge Not done 100%) as Air Plug gauge Unit is under calibration | O |
Machine | In Deburring no contribution for hole oversize | No Contribution | X |
Tool | In Blanking/Piercing Premachining Hole | We have verified after blanking operation Premachining hole is ok | X |
Method | In Machining its chance to mix up the part (Setting Part/Rework part) | Yes its having possibility to mixup the rejected parts (Setting Parts)at machine stage | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | In CNC machining ID Oversize by 0.2 |
Why 2 | 100% Air Gauge parts not checked |
Why 3 | Setting Part get mix up by operator |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Due to there is no Red Bin Available at machine stage so Rejected parts get mixed up |
Root Cause Analysis (Outflow)
Why 1 | As 100% Air Plug gauge Checking at Final Stage as well as Machine stage |
Why 2 | 100% Plug gauge not Done for final inspection |
Why 3 | As Air gauge unit is under Calibration so that 100% inspection not done at final stage |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | As Air Gauge Unit is under calibration so that 100% inspection not done at final stage |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Now we have kept Red bin with lock and key for rejection parts (Set up /rework parts) | Mr. Gaurav Nikam | 05/09/2022 | Completed | |
Outflow | Duble Ended Plain Plug Gauge (Carbide Go) 26.020-26.041 procured as contingency of Air Gauge Unit (if Air gauge unit is under calibration so far used PPG for 100% Inspection at Final Inspection Stage) | Mr. Gaurav Nikam | 05/09/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No Changed |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
Due to there is no Red Bin Available at machine stage so Rejected parts get mixed up 231_Occurance_Before.xlsx |
Occurance (After) |
Now we have kept Red bin with lock and key for rejection parts (Set up /rework parts) 231_Occurance_After.xlsx |
Outflow (Before) |
As Air Gauge Unit is under calibration so that 100% inspection not done at final stage 231_Outflow_Before.xlsx |
Outflow (After) |
Duble Ended Plain Plug Gauge (Carbide Go) 26.020-26.041 procured as contingency of Air Gauge Unit (if Air gauge unit is under calibration so far used PPG for 100% Inspection at Final Inspection Stage) 231_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | |
Specify Other Document | No Any Other Documen |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |