QFR No - 8000802401
Defect Details
NC No. 8000802401
NC Date 31/08/2022
NC Submission Date
Part No. S2HT11807B
Part Name OUTER SPRING _B104 E
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details POWDER COATING NOT OK-P.COATING ROUGHESS&SHSDE VERACTION
 
1. Problem Description
Defect Description Powder coating Uncover & shade variation due to Over backing
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 190
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID ravindra@helicalsprings.in
Plant Head/CEO Email ID shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
0
0
0
2000
3500
Check Qty
1500
0
0
0
2000
3500
NG Qty
190
0
0
0
0
190
 
Scrap 0
Rework 190
Under Deviation 0
Containment Action
Check all material ETL end & helical end.
 
3. Process Flow
Process Flow Description
Raw Material Receipt & Inspection> Coiling > Stress Relieving > End Grinding > Shot Peening > Scragging > ID, Length & Angle checking > Surface Finish- Powder Coating > Final Inspection/ PDI > Packing > Dispatch
 
4. Process Details
Process / Operation Powder Coating
Outsource No
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine check Sheet not followedCLIT verified found OkO
MethodImproper Material handlingMaterial handling done as per process verified found okO
Manunskilled OperatorSkill matrix checked found okO
MaterialMaterial GradeRMTC verified found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1000/19
7. Root Cause Analysis (Occurance)
Why 1 Powder Coating Shade Varication
Why 2 Imbalance mixing ratio of fresh & recycle powder
Why 3
Why 4
Why 5
Root Cause (Occurance) Imbalance mixing ratio of fresh & recycle powder
 
Root Cause Analysis (Outflow)
Why 1 Powder Coating Shade varicaton
Why 2 PDIR done sampling basis
Why 3 Not Detect in sampling
Why 4
Why 5
Root Cause (Outflow) Not Detect in sampling
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceMixing ratio of fresh & recycle powder defined: 80 - 20 %Mr. Narayan Shedute30/09/202214/09/2022Completed
OutflowMaster samples & panels madeMr.Anuj Shelke30/09/202214/09/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection done before dispatch.
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 1000/25
10. Evidance of Countermeasure
Occurance (Before) Mixing ratio of fresh & recycle powder was 70- 30 %
236_Occurance_Before.pdf
Occurance (After) Mixing ratio of fresh & recycle powder defined: 80 - 20 %
236_Occurance_After.pdf
Outflow (Before) Criteria was not defined for shade
236_Outflow_Before.pdf
Outflow (After) Master samples & panels made
236_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant B104 Outer & B106 Big (Brass Gold Coated Part only.)
 
12. Document Review
Documents WISOP
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission No Defect reported