QFR No - 8000802986
Defect Details
NC No. 8000802986
NC Date 06/09/2022
NC Submission Date
Part No. 520FG07802
Part Name GEAR PRIMARY DRIVEN (JZ)
Supplier Name & Code 200172-AURANGABAD AUTO ENGG PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details PCD SHIFT-SPRING SPOKET& 3BOSS PCD NOT OK
 
1. Problem Description
Defect Description Spring Pocket PCD & Concentricity not OK
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 94
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID verma.aaepl@gmail.com
Plant Head/CEO Email ID aaepl.pantnagar@sangkaj.com
MD Email ID steel@sangkaj.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2150
0
0
2588
3500
8238
Check Qty
1150
0
0
2588
3500
7238
NG Qty
2
0
0
0
16
18
 
Scrap 0
Rework 16
Under Deviation 0
Containment Action
100 % WIP And Customer end all part rechecked by PCD relation gauge
 
3. Process Flow
Process Flow Description
Forging -CNC 1at setup - CNC 2nd Setup -Trimming - Kidney pocket deburring - CNC 1st setup - CNC 2nd Setup - Inspection -Hobbing -HT-ID Honning -Teeth Honning -Final Inspection - Dispatch
 
4. Process Details
Process / Operation Trimming
Outsource Yes
Machine / Cell Trimming Press Machine
Machine / Cell No. CNC Cell
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineJaw boring not done as per frequencyJaw boring frequency not followO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5/Per lot
7. Root Cause Analysis (Occurance)
Why 1 Part not answering to relation gauge
Why 2 Window location shifted
Why 3 Jaw boring out
Why 4 Jaw boring not done as per frequency
Why 5
Root Cause (Occurance) Jaw boring frequency not follow as control plan
 
Root Cause Analysis (Outflow)
Why 1 Sampling inspection done at final stage
Why 2 Inspection done as per control plan
Why 3
Why 4
Why 5
Root Cause (Outflow) Sampling inspection done at final inspection stage
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceJaw boring cycle interlockedProduction In charge16/12/202215/12/2022Completed
Outflow100% inspection startedfinal inspector20/12/202212/12/2022Completed
Occurance100% inspection started at final inspection stage by relation gaugeFinal Inspector01/12/202209/12/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Before we have checked on sampling basis after Complaint received we have started 100% inspection .
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Jaw boring not done as per frequency
247_Occurance_Before.xlsx
Occurance (After) Interlock implemented for jaw boring frequency monitoring
247_Occurance_After.xlsx
Outflow (Before) Sampling Inspection at final stage
247_Outflow_Before.xlsx
Outflow (After) 100% Inspection done at final inspection stage
247_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant DX101004 - Gear Primary Driven
 
12. Document Review
Documents ControlPlan, JHCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 3000
Reason for submission OK