QFR No - 8000802986
Defect Details
NC No. | 8000802986 |
NC Date | 06/09/2022 |
NC Submission Date | |
Part No. | 520FG07802 |
Part Name | GEAR PRIMARY DRIVEN (JZ) |
Supplier Name & Code | 200172-AURANGABAD AUTO ENGG PVT LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | PCD SHIFT-SPRING SPOKET& 3BOSS PCD NOT OK |
1. Problem Description
Defect Description | Spring Pocket PCD & Concentricity not OK |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 94 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | verma.aaepl@gmail.com |
Plant Head/CEO Email ID | aaepl.pantnagar@sangkaj.com |
MD Email ID | steel@sangkaj.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2150
|
0
|
0
|
2588
|
3500
|
8238
|
Check Qty |
1150
|
0
|
0
|
2588
|
3500
|
7238
|
NG Qty |
2
|
0
|
0
|
0
|
16
|
18
|
Scrap | 0 |
Rework | 16 |
Under Deviation | 0 |
Containment Action |
---|
100 % WIP And Customer end all part rechecked by PCD relation gauge |
3. Process Flow
Process Flow Description |
---|
Forging -CNC 1at setup - CNC 2nd Setup -Trimming - Kidney pocket deburring - CNC 1st setup - CNC 2nd Setup - Inspection -Hobbing -HT-ID Honning -Teeth Honning -Final Inspection - Dispatch |
4. Process Details
Process / Operation | Trimming |
Outsource | Yes |
Machine / Cell | Trimming Press Machine |
Machine / Cell No. | CNC Cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Jaw boring not done as per frequency | Jaw boring frequency not follow | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5/Per lot |
7. Root Cause Analysis (Occurance)
Why 1 | Part not answering to relation gauge |
Why 2 | Window location shifted |
Why 3 | Jaw boring out |
Why 4 | Jaw boring not done as per frequency |
Why 5 | |
Root Cause (Occurance) | Jaw boring frequency not follow as control plan |
Root Cause Analysis (Outflow)
Why 1 | Sampling inspection done at final stage |
Why 2 | Inspection done as per control plan |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Sampling inspection done at final inspection stage |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Jaw boring cycle interlocked | Production In charge | 16/12/2022 | 15/12/2022 | Completed |
Outflow | 100% inspection started | final inspector | 20/12/2022 | 12/12/2022 | Completed |
Occurance | 100% inspection started at final inspection stage by relation gauge | Final Inspector | 01/12/2022 | 09/12/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Before we have checked on sampling basis after Complaint received we have started 100% inspection . |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Jaw boring not done as per frequency 247_Occurance_Before.xlsx |
Occurance (After) |
Interlock implemented for jaw boring frequency monitoring 247_Occurance_After.xlsx |
Outflow (Before) |
Sampling Inspection at final stage 247_Outflow_Before.xlsx |
Outflow (After) |
100% Inspection done at final inspection stage 247_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | DX101004 - Gear Primary Driven |
12. Document Review
Documents | ControlPlan, JHCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 3000 |
Reason for submission | OK |