QFR No - 8000805728
Defect Details
NC No. 8000805728
NC Date 26/09/2022
NC Submission Date
Part No. 520AM01202
Part Name BALL RACE
Supplier Name & Code 100264-SAI INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CORE DEPTH AND SURFACE HARDNESS NOT OK
 
1. Problem Description
Defect Description Case depth and surface hardness found not ok
Detection Stage Receipt
Problem Severity Function
NG Quantity 2060
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID info@sai-industries.com
Plant Head/CEO Email ID info@sai-industries.com
MD Email ID umesh.honap@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2060
0
0
0
0
2060
Check Qty
2060
0
0
0
0
2060
NG Qty
2060
0
0
0
0
2060
 
Scrap 2060
Rework 0
Under Deviation 0
Containment Action
Verified in ETL found 60 nos. crack during assly. in 1200 Nos. After received in Sai will be scraped. In Logistic and in house No finish stock verify for crack. Information has been given to heat treatment supplier for minimize case depth and core hardness.
 
3. Process Flow
Process Flow Description
R/M - Cutting - Drilling - CNC Turning - Heat Treatment-C`less Grinding-Track & I/D Finish-Final Inspection-Packing & Dispatch.
 
4. Process Details
Process / Operation Heat Treatment
Outsource Yes
Machine / Cell Furnace
Machine / Cell No. Furnace
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Man--X
Tool--X
MethodCarburising cycle time and quenching temperature excess than specification found.Carburising cycle time and quenching temperature excess than specification found.O
Material--X
Machine--X
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size One\Lot
7. Root Cause Analysis (Occurance)
Why 1 Ball Race crack during assly. "
Why 2 In destructive testing case depth and core harness is above specification.
Why 3 Case depth found 1.20 and core hardness found 57RC.
Why 4 In heat treatment cycle not followed by supplier.
Why 5 Carburizing cycle time and quenching temperature excess than specification observed.
Root Cause (Occurance) Carburizing cycle time and quenching temperature excess than specification found.
 
Root Cause Analysis (Outflow)
Why 1 Ball Race crack during assly.
Why 2 In Final Inspection above defect not detect.
Why 3 Due to destructive testing parts not verify before frequency.
Why 4 Destructive testing frequency not adequate. Currently is once In Six Month.
Why 5
Root Cause (Outflow) Destructive testing frequency not adequate. Currently is once In Six Month.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceRevised heat tretament control plan for to minimize Carburizing cycle time and quenching low temperature implemented . Carburising cycle(soaking) time changed 70 to 60 Minutes.Quenching temperature changed 860 to 850°C.Trial conducted for one lot & supplied with green dot mark on o/d 48 as identification.Supplier & Sai25/09/202226/09/2022Completed
OutflowOne piece test quarterly in NABL lab for Case depth & Core Hardness started. Corrected one lot 500 nos.supplied to ETL with green dot on o/d 48 as a indetification mark.NABL lab report submitted along with lot.Sai26/09/202226/09/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details -
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size One\Lot
10. Evidance of Countermeasure
Occurance (Before) CHT Cycle Carburizing cycle time - 70 Minutes. Quenching teperature - 860°C
264_Occurance_Before.pdf
Occurance (After) CHT Cycle Carburizing cycle time - 60 Minutes. Quenching teperature - 850°C
264_Occurance_After.pdf
Outflow (Before) 3 rd Party inspection Frequency 6 month
264_Outflow_Before.pdf
Outflow (After) 3 rd Party inspection frequency 3 Month
264_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Ball Race Regular
 
12. Document Review
Documents ControlPlan
Specify Other Document -
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission ok