QFR No - 8000807048
Defect Details
NC No. 8000807048
NC Date 08/10/2022
NC Submission Date
Part No. B2GQ01003O
Part Name MASTER CYLINDER BODY PDC RAW-K11,K2
Supplier Name & Code 100471-CASTALL TECHNOLOGIES (P) LTD
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details DIMENSSIONAL DEFECT-SLOT WIDTH O/S BY 0.2 MM
 
1. Problem Description
Defect Description SLOT WIDTH O/S BY 0.2 MM
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qa@castalltech.com
Plant Head/CEO Email ID sg@castalltech.com
MD Email ID nmv@castalltech.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
1050
0
1050
Check Qty
0
0
0
1050
0
1050
NG Qty
0
0
0
1
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
100% checked at vendors site
 
3. Process Flow
Process Flow Description
Operation # 50
 
4. Process Details
Process / Operation PDC
Outsource No
Machine / Cell PDC 400
Machine / Cell No. PDC 5
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Manpart mix up , slippage of gauge checkingverifiedO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Excess fettling
Why 2 gauge not checked after fettling
Why 3 operators awareness
Why 4
Why 5
Root Cause (Occurance) Gauging after fettling to be assured by training and awareness program for the fettling team
 
Root Cause Analysis (Outflow)
Why 1 Part mixed up in final inspection
Why 2 No partition in final inspection table for "to be inspected " and "Inspected OK " area
Why 3 No visual aid and no identification mark after gauge checking
Why 4
Why 5
Root Cause (Outflow) Partition implemented in Final Inspection area. Visual aid provided, parts identified with mark after 100% gauge checking
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowPartition implemented for "To be Inspected" and "Inspected OK " partsQA09/08/202223/08/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Change implemented with on job training of the inspector
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) part mixed up
281_Occurance_Before.jpeg
Occurance (After) Partition provided
281_Occurance_After.jpeg
Outflow (Before) Without identification
281_Outflow_Before.jpeg
Outflow (After) 100% gauge checking with identification, Visual aid provided
281_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Master cylinders variants
 
12. Document Review
Documents WISOP
Specify Other Document Visual aid
 
13. Effectiveness Of Action
Reviewed Quantity 200
Reason for submission No Same defective parts found in received last lot