QFR No - 8000807218
Defect Details
NC No. 8000807218
NC Date 08/10/2022
NC Submission Date
Part No. 550LG06202
Part Name SEAT PIPE -K23A/PRFH-006
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1116-ETL K-120 Suspension
Defect Details THREADING NOT OK-THREAD GO GAUGE NOT ENTERED.
 
1. Problem Description
Defect Description Threading M8 observed not Ok (Go gauge not entered.) Concern repetitively communicated from last six months, but yet no any improvement observed in received lots.
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 3000
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5600
1000
0
0
0
6600
Check Qty
5600
1000
0
0
0
6600
NG Qty
3000
200
0
0
0
3200
 
Scrap 0
Rework 3200
Under Deviation 0
Containment Action
Segregated all parts at ETL, at Warehouse & at NPC Nabha.
 
3. Process Flow
Process Flow Description
Process Flow Description 1.Raw Material 2.Cutting & Chemfering 3. Multistation Draw 4.Head Formation 5.Rough Grinding 6.Punching 7.CNC Head Turning 8.CNC Boring & Facing 9.Tapping 10. Chemfering 1&2 11.Finish Grinding 12.Final Inspection 13.Cleaning 14.Oiling 15.Packing &Dispatch
 
4. Process Details
Process / Operation Tapping
Outsource Yes
Machine / Cell tapping machine
Machine / Cell No. NPC/CNC/011
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Methodskipped at final inspectionit was observed that parts skipped during sampling at final inspection.X
ManOperator negligence at in processoperator was aware about the defect he found to be non negligentO
MethodChips in threadAfter validation no chips found in threadO
MethodMinor Dia u/safter verification we found okO
MaterialMaterial Hardness less / moreafter verification we found okO
MethodTap Wear Outafter verification we found tap was wear outX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size asper plan
7. Root Cause Analysis (Occurance)
Why 1 M8 GO TPG not answering
Why 2 Wear out tapping tool used in process.
Why 3 Operator was less awareness about the tapping tool
Why 4 New operator appointed and training gap observed
Why 5
Root Cause (Occurance) New operator appointed and training gap observed
 
Root Cause Analysis (Outflow)
Why 1 M8 GO TPG not answering
Why 2 Could not be detected at Final Inspection
Why 3 Skipped in Sampling at Final Inspection
Why 4 Less quantity in our Sampling at Final Inspection
Why 5
Root Cause (Outflow) Less quantity in our Sampling at Final Inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTPG Inspection to be done after every 60pcs(or 10minutes) by operator.Mr. Rajinder08/11/202202/11/2022Completed
OutflowIncrease sampling size at Final inspection.Mr. Yadvinder16/10/202213/10/2022Completed
OccuranceTraining to be provided to new operator about the process any new station.Mr. Gurpreet Singh08/11/202202/11/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Increase sampling size at Final inspection.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size asper plan
10. Evidance of Countermeasure
Occurance (Before) New operator appointed and training gap observed
277_Occurance_Before.jpg
Occurance (After) Training to be provided to new operator about the process any new station.
277_Occurance_After.jpg
Outflow (Before) Less quantity in our Sampling at Final Inspection
277_Outflow_Before.jpg
Outflow (After) Increase sampling size at Final inspection.
277_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant DRILLING MACHINE
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PokayokeCheckSheet, WISOP, JHCheckSheet, AuditCheckSheet, InspCheckSheet
Specify Other Document TRAINING SHEET
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission Completed.